| Assessment Year | 1988 |
|---|---|
| Principal Product | FROZEN CHICKEN PIECES |
| NAICS |
n/a
|
| SIC | 2015: Poultry Slaughtering and Processing |
| Sales Range | $50 M to 100M |
| # of Employees | 1,000 |
| Plant Area |
n/a
|
| Annual Production | 150,000,000
pieces
|
| Production Hrs. Annual | 8,400
hrs
|
| Location (State) | Arkansas |
Facility Energy Cost and Usage
| Source | Yearly Cost | Usage | Unit Cost | |
|---|---|---|---|---|
| Electricity Usage | $833,170 | 23,448,125 |
kWh
|
$0.036 |
| Natural Gas | $288,964 | 103,963 |
MMBtu
|
$2.78 |
| TOTAL YEARLY COSTS | - | |||
| RECOMMENDED SAVINGS* | $36,382 |
See individual recommendations below
*Non-energy impacts included in savings.
|
||
| IMPLEMENTED SAVINGS* | $28,715 | |||
Recommendations
| # | Description | Yearly Savings* | Imp'd Cost* | Status | Electricity Usage Savings | Natural Gas Savings |
|---|---|---|---|---|---|---|
| 01 | 2.7142: Utilize higher efficiency lamps and/or ballasts | $4,200 | $1,575 |
$4,200
143,904
kWh
|
- | |
| 02 | 2.7142: Utilize higher efficiency lamps and/or ballasts | $1,960 | $2,787 |
$1,960
67,116
kWh
|
- | |
| 03 | 2.2122: Install / repair insulation on condensate lines | $642 | $184 | - |
$642
-
MMBtu
|
|
| 04 | 2.2511: Insulate bare equipment | $728 | $312 | - |
$728
-
MMBtu
|
|
| 05 | 2.2136: Install / repair insulation on steam lines | $2,028 | $2,050 | - |
$2,028
-
MMBtu
|
|
| 06 | 2.2515: Use optimum thickness insulation | $761 | $1,380 |
$761
32,239
kWh
|
- | |
| 07 | 2.2135: Repair and eliminate steam leaks | $4,601 | $300 | - |
$4,601
-
MMBtu
|
|
| 08 | 2.4322: Use or replace with energy efficient substitutes | $11,976 | $405 |
$(-120.0)
(-4,103)
kWh
|
$12,096
-
MMBtu
|
|
| 09 | 2.4133: Use most efficient type of electric motors | $1,819 | $2,370 |
$1,819
55,686
kWh
|
- | |
| 10 | 2.2449: Recover heat from exhausted steam, hot air or hot water | $7,667 | $5,510 | - |
$7,667
-
MMBtu
|
|
| TOTAL RECOMMENDED | $36,382 | $16,873 |
$8,620
294,842
kWh
|
$27,762
-
MMBtu
|
||
| TOTAL IMPLEMENTED | $28,715 | $11,363 |
$8,620
294,842
kWh
|
$20,095
-
MMBtu
|
||
| Yearly Savings* | Imp'd Cost* | Electricity Usage Savings | Natural Gas Savings | |||
*Savings and costs are best estimates based on the center's site visit, associated engineering analysis, and typical capital and labor costs