Assessment Year | 2017 |
---|---|
Principal Product | Corrugated and Solid Fiber Box Manufacturing |
NAICS | 322211: Corrugated and Solid Fiber Box Manufacturing |
SIC | 2653: Corrugated and Solid Fiber Boxes |
Sales Range | $10 M to 50M |
# of Employees | 53 |
Plant Area |
230,000
ft2
|
Annual Production | 200,000
thousand feet
|
Production Hrs. Annual | 2,250
hrs
|
Location (State) | Nebraska |
Facility Energy Cost and Usage
Source | Yearly Cost | Usage | Unit Cost | |
---|---|---|---|---|
Electricity Usage | $56,077 | 1,211,904 |
kWh
|
$0.046 |
Electricity Demand | $69,863 | 7,000 |
kW-mo/yr
|
$9.98 |
Electricity Fees | $6,141 | - |
|
- |
Natural Gas | $45,789 | 7,680 |
MMBtu
|
$5.96 |
TOTAL YEARLY COSTS | $177,870 | |||
RECOMMENDED SAVINGS* | $13,738 |
See individual recommendations below
*Non-energy impacts included in savings.
|
||
IMPLEMENTED SAVINGS* | $5,729 |
Recommendations
# | Description | Yearly Savings* | Imp'd Cost* | Status | Electricity Usage Savings | Electricity Demand Savings | Personnel Changes Savings |
---|---|---|---|---|---|---|---|
01 | 2.3131: Reschedule plant operations or reduce load to avoid peaks | $6,874 | - | - |
$6,874
-
kW-mo/yr
|
- | |
02 | 2.7142: Utilize higher efficiency lamps and/or ballasts | $4,747 | $20,139 |
$2,282
49,350
kWh
|
$2,465
-
kW-mo/yr
|
- | |
03 | 2.4236: Eliminate leaks in inert gas and compressed air lines/ valves | $1,135 | $1,571 |
$1,579
34,118
kWh
|
- | $(-444.0) | |
04 | 3.1291: Eliminate practice of mixing waste streams | $982 | - |
$982
21,356
kWh
|
- | - | |
TOTAL RECOMMENDED | $13,738 | $21,710 |
$4,843
104,824
kWh
|
$9,339
-
kW-mo/yr
|
$(-444.0) | ||
TOTAL IMPLEMENTED | $5,729 | $20,139 |
$3,264
70,706
kWh
|
$2,465
-
kW-mo/yr
|
- |
*Savings and costs are best estimates based on the center's site visit, associated engineering analysis, and typical capital and labor costs