Assessment Year | 2017 |
---|---|
Principal Product | treated municipal and industrial wastewater |
NAICS | 221320: Sewage Treatment Facilities |
SIC | 4952: Sewerage Systems |
Sales Range | $1 M to 5M |
# of Employees | 10 |
Plant Area |
34,170
ft2
|
Annual Production | 1,992,900
Tgal
|
Production Hrs. Annual | 8,760
hrs
|
Location (State) | Nebraska |
Facility Energy Cost and Usage
Source | Yearly Cost | Usage | Unit Cost | |
---|---|---|---|---|
Electricity Usage | $150,981 | 5,591,896 |
kWh
|
$0.027 |
Electricity Demand | $68,484 | 11,890 |
kW-mo/yr
|
$5.76 |
Electricity Fees | $3,145 | - |
|
- |
LPG | $13,950 | 15,000 |
MMBtu
|
$0.93 |
TOTAL YEARLY COSTS | $236,560 | |||
RECOMMENDED SAVINGS* | $147,150 |
See individual recommendations below
*Non-energy impacts included in savings.
|
||
IMPLEMENTED SAVINGS* | $800 |
Recommendations
# | Description | Yearly Savings* | Imp'd Cost* | Status | Electricity Usage Savings | Electricity Demand Savings | Primary Raw Material Savings | Increase in Production Savings |
---|---|---|---|---|---|---|---|---|
01 | 2.4322: Use or replace with energy efficient substitutes | $106,860 | $650,000 |
$7,891
289,056
kWh
|
$6,083
-
kW-mo/yr
|
$16,236 | $76,650 | |
02 | 2.1311: Replace electrically-operated equipment with fossil fuel equipment | $35,435 | $57,984 |
$26,020
953,109
kWh
|
$9,415
-
kW-mo/yr
|
- | - | |
03 | 2.4239: Eliminate or reduce compressed air usage | $4,055 | $60,000 |
$3,024
110,769
kWh
|
$1,031
-
kW-mo/yr
|
- | - | |
04 | 2.7142: Utilize higher efficiency lamps and/or ballasts | $800 | $6,424 |
$800
29,292
kWh
|
- | - | - | |
TOTAL RECOMMENDED | $147,150 | $774,408 |
$37,735
1,382,226
kWh
|
$16,529
-
kW-mo/yr
|
$16,236 | $76,650 | ||
TOTAL IMPLEMENTED | $800 | $6,424 |
$800
29,292
kWh
|
- | - | - |
*Savings and costs are best estimates based on the center's site visit, associated engineering analysis, and typical capital and labor costs