| Assessment Year | 2017 |
|---|---|
| Principal Product | treated municipal and industrial wastewater |
| NAICS | 221320: Sewage Treatment Facilities |
| SIC | 4952: Sewerage Systems |
| Sales Range | $1 M to 5M |
| # of Employees | 10 |
| Plant Area |
34,170
ft2
|
| Annual Production | 1,992,900
Tgal
|
| Production Hrs. Annual | 8,760
hrs
|
| Location (State) | Nebraska |
Facility Energy Cost and Usage
| Source | Yearly Cost | Usage | Unit Cost | |
|---|---|---|---|---|
| Electricity Usage | $150,981 | 5,591,896 |
kWh
|
$0.027 |
| Electricity Demand | $68,484 | 11,890 |
kW-mo/yr
|
$5.76 |
| Electricity Fees | $3,145 | - |
|
- |
| LPG | $13,950 | 15,000 |
MMBtu
|
$0.93 |
| TOTAL YEARLY COSTS | $236,560 | |||
| RECOMMENDED SAVINGS* | $147,150 |
See individual recommendations below
*Non-energy impacts included in savings.
|
||
| IMPLEMENTED SAVINGS* | $800 | |||
Recommendations
| # | Description | Yearly Savings* | Imp'd Cost* | Status | Electricity Usage Savings | Electricity Demand Savings | Primary Raw Material Savings | Increase in Production Savings |
|---|---|---|---|---|---|---|---|---|
| 01 | 2.4322: Use or replace with energy efficient substitutes | $106,860 | $650,000 |
$7,891
289,056
kWh
|
$6,083
-
kW-mo/yr
|
$16,236 | $76,650 | |
| 02 | 2.1311: Replace electrically-operated equipment with fossil fuel equipment | $35,435 | $57,984 |
$26,020
953,109
kWh
|
$9,415
-
kW-mo/yr
|
- | - | |
| 03 | 2.4239: Eliminate or reduce compressed air usage | $4,055 | $60,000 |
$3,024
110,769
kWh
|
$1,031
-
kW-mo/yr
|
- | - | |
| 04 | 2.7142: Utilize higher efficiency lamps and/or ballasts | $800 | $6,424 |
$800
29,292
kWh
|
- | - | - | |
| TOTAL RECOMMENDED | $147,150 | $774,408 |
$37,735
1,382,226
kWh
|
$16,529
-
kW-mo/yr
|
$16,236 | $76,650 | ||
| TOTAL IMPLEMENTED | $800 | $6,424 |
$800
29,292
kWh
|
- | - | - | ||
*Savings and costs are best estimates based on the center's site visit, associated engineering analysis, and typical capital and labor costs