| Assessment Year | 2017 |
|---|---|
| Principal Product | Beef jerky |
| NAICS | 311612: Meat Processed from Carcasses |
| SIC | 2013: Sausages and Other Prepared Meat Products |
| Sales Range | $50 M to 100M |
| # of Employees | 500 |
| Plant Area |
140,000
ft2
|
| Annual Production | 10,000,000
pieces
|
| Production Hrs. Annual | 4,000
hrs
|
| Location (State) | Virginia |
Facility Energy Cost and Usage
| Source | Yearly Cost | Usage | Unit Cost | ||
|---|---|---|---|---|---|
| Electricity Usage | $368,874 | 11,711,000 |
kWh
|
$0.031 | |
| Electricity Demand | $474,223 | 24,922 |
kW-mo/yr
|
$19.03 | |
| Natural Gas | $330,951 | 47,440 |
MMBtu
|
$6.98 | |
| Waste Disposal Costs | |||||
| Water Usage | $592,592 | 27,524 |
Tgal
|
$21.53 | |
| TOTAL YEARLY COSTS | $1,766,640 | ||||
| RECOMMENDED SAVINGS* | $49,978 |
See individual recommendations below
*Non-energy impacts included in savings.
|
|||
| IMPLEMENTED SAVINGS* | $5,049 | ||||
Recommendations
| # | Description | Yearly Savings* | Imp'd Cost* | Status | Electricity Usage Savings | Electricity Demand Savings | Natural Gas Savings | Water Usage Savings | Personnel Changes Savings | Ancillary Material Cost Savings |
|---|---|---|---|---|---|---|---|---|---|---|
| 01 | 2.4236: Eliminate leaks in inert gas and compressed air lines/ valves | $2,641 | $200 |
$1,397
49,191
kWh
|
$1,444
-
kW-mo/yr
|
- | - | $(-100.0) | $(-100.0) | |
| 02 | 2.4239: Eliminate or reduce compressed air usage | $1,840 | $750 |
$906
31,893
kWh
|
$934
-
kW-mo/yr
|
- | - | - | - | |
| 03 | 2.4231: Reduce the pressure of compressed air to the minimum required | $1,606 | $100 |
$792
27,888
kWh
|
$814
-
kW-mo/yr
|
- | - | - | - | |
| 04 | 2.1232: Keep boiler tubes clean | $2,408 | $1,000 | - | - |
$2,408
-
MMBtu
|
- | - | - | |
| 05 | 2.2123: Insulate feedwater tank | $792 | $750 | - | - |
$792
-
MMBtu
|
- | - | - | |
| 06 | 2.2437: Recover waste heat from equipment | $15,825 | $82,000 | - | - |
$15,825
-
MMBtu
|
- | - | - | |
| 07 | 4.212: Adopt in-house material generation | $21,773 | $20,000 |
$(-1,861.0)
(-65,541)
kWh
|
$(-4,017.0)
-
kW-mo/yr
|
- | - | - | $27,651 | |
| 08 | 2.7135: Install occupancy sensors | $217 | $487 |
$173
6,079
kWh
|
$44
-
kW-mo/yr
|
- | - | - | - | |
| 09 | 3.4156: Use flow control valves on equipment to optimize water use | $2,876 | $30 | - | - | - |
$2,876
-
Tgal
|
- | - | |
| TOTAL RECOMMENDED | $49,978 | $105,317 |
$1,407
49,510
kWh
|
$(-781.0)
-
kW-mo/yr
|
$19,025
-
MMBtu
|
$2,876
-
Tgal
|
$(-100.0) | $27,551 | ||
| TOTAL IMPLEMENTED | $5,049 | $1,200 |
$1,397
49,191
kWh
|
$1,444
-
kW-mo/yr
|
$2,408
-
MMBtu
|
- | $(-100.0) | $(-100.0) | ||
| Yearly Savings* | Imp'd Cost* | Electricity Usage Savings | Electricity Demand Savings | Natural Gas Savings | Water Usage Savings | Personnel Changes Savings | Ancillary Material Cost Savings | |||
*Savings and costs are best estimates based on the center's site visit, associated engineering analysis, and typical capital and labor costs