Assessment Year | 2014 |
---|---|
Principal Product | Upholstered furniture |
NAICS | 337121: Upholstered Household Furniture Manufacturing |
SIC | 2512: Wood Household Furniture, Upholstered |
Sales Range | $5 M to 10M |
# of Employees | 75 |
Plant Area |
105,000
ft2
|
Annual Production | 12,000
pieces
|
Production Hrs. Annual | 2,000
hrs
|
Location (State) | North Carolina |
Facility Energy Cost and Usage
Source | Yearly Cost | Usage | Unit Cost | |
---|---|---|---|---|
Electricity Usage | $78,588 | 1,589,280 |
kWh
|
$0.049 |
Electricity Demand | $45,876 | 3,888 |
kW-mo/yr
|
$11.80 |
Electricity Fees | $101 | - |
|
- |
Natural Gas | $6,398 | 700 |
MMBtu
|
$9.14 |
TOTAL YEARLY COSTS | - | |||
RECOMMENDED SAVINGS* | $14,910 |
See individual recommendations below
*Non-energy impacts included in savings.
|
||
IMPLEMENTED SAVINGS* | $12,735 |
Recommendations
# | Description | Yearly Savings* | Imp'd Cost* | Status | Electricity Usage Savings | Electricity Demand Savings | Natural Gas Savings | Ancillary Material Cost Savings |
---|---|---|---|---|---|---|---|---|
01 | 2.8114: Change rate schedules or other changes in utility service | $6,707 | $1,000 |
$(-22,873.0)
-
kWh
|
$29,580
-
kW-mo/yr
|
- | - | |
02 | 2.7111: Reduce illumination to minimum necessary levels | $1,152 | $157 |
$433
8,650
kWh
|
$612
-
kW-mo/yr
|
- | $107 | |
03 | 2.7142: Utilize higher efficiency lamps and/or ballasts | $3,187 | $1,625 |
$1,318
26,352
kWh
|
$1,869
-
kW-mo/yr
|
- | - | |
04 | 2.7135: Install occupancy sensors | $411 | $697 |
$411
8,217
kWh
|
- | - | - | |
05 | 2.7142: Utilize higher efficiency lamps and/or ballasts | $798 | $3,231 |
$333
6,664
kWh
|
$472
-
kW-mo/yr
|
- | $(-7.0) | |
06 | 2.2123: Insulate feedwater tank | $198 | $75 | - | - |
$198
-
MMBtu
|
- | |
07 | 2.2136: Install / repair insulation on steam lines | $792 | $787 | - | - |
$792
-
MMBtu
|
- | |
08 | 2.4231: Reduce the pressure of compressed air to the minimum required | $585 | $50 |
$242
4,845
kWh
|
$343
-
kW-mo/yr
|
- | - | |
09 | 2.2437: Recover waste heat from equipment | $725 | $450 | - | - |
$725
-
MMBtu
|
- | |
10 | 2.4236: Eliminate leaks in inert gas and compressed air lines/ valves | $270 | $100 |
$112
2,238
kWh
|
$158
-
kW-mo/yr
|
- | - | |
11 | 2.4239: Eliminate or reduce compressed air usage | $85 | $105 |
$85
1,632
kWh
|
- | - | - | |
TOTAL RECOMMENDED | $14,910 | $8,277 |
$(-19,939.0)
58,598
kWh
|
$33,034
-
kW-mo/yr
|
$1,715
-
MMBtu
|
$100 | ||
TOTAL IMPLEMENTED | $12,735 | $4,209 |
$(-20,514.0)
47,089
kWh
|
$32,219
-
kW-mo/yr
|
$923
-
MMBtu
|
$107 | ||
Yearly Savings* | Imp'd Cost* | Electricity Usage Savings | Electricity Demand Savings | Natural Gas Savings | Ancillary Material Cost Savings |
*Savings and costs are best estimates based on the center's site visit, associated engineering analysis, and typical capital and labor costs