Assessment Year | 2013 |
---|---|
Principal Product | Circuit boards |
NAICS | 334418: Printed Circuit Assembly (Electronic Assembly) Manufacturing |
SIC | 3679: Electronic Components, Not Elsewhere Classified |
Sales Range | $10 M to 50M |
# of Employees | 117 |
Plant Area |
60,000
ft2
|
Annual Production | 8,000,000
pieces
|
Production Hrs. Annual | 2,100
hrs
|
Location (State) | North Carolina |
Facility Energy Cost and Usage
Source | Yearly Cost | Usage | Unit Cost | |
---|---|---|---|---|
Electricity Usage | $75,581 | 1,059,394 |
kWh
|
$0.071 |
Electricity Demand | $12,915 | 3,150 |
kW-mo/yr
|
$4.10 |
Electricity Fees | $509 | - |
|
- |
Natural Gas | $12,064 | 1,470 |
MMBtu
|
$8.21 |
TOTAL YEARLY COSTS | - | |||
RECOMMENDED SAVINGS* | $7,872 |
See individual recommendations below
*Non-energy impacts included in savings.
|
||
IMPLEMENTED SAVINGS* | $6,823 |
Recommendations
# | Description | Yearly Savings* | Imp'd Cost* | Status | Electricity Usage Savings | Electricity Demand Savings | Natural Gas Savings | Personnel Changes Savings | Ancillary Material Cost Savings |
---|---|---|---|---|---|---|---|---|---|
01 | 2.4231: Reduce the pressure of compressed air to the minimum required | $686 | $25 |
$499
7,938
kWh
|
$187
-
kW-mo/yr
|
- | - | - | |
02 | 2.6218: Turn off equipment when not in use | $333 | $50 |
$333
5,287
kWh
|
- | - | - | - | |
03 | 2.4236: Eliminate leaks in inert gas and compressed air lines/ valves | $103 | $100 |
$177
2,820
kWh
|
$66
-
kW-mo/yr
|
- | $(-100.0) | $(-40.0) | |
04 | 2.2437: Recover waste heat from equipment | $363 | $850 | - | - |
$363
-
MMBtu
|
- | - | |
05 | 2.7111: Reduce illumination to minimum necessary levels | $618 | $300 |
$374
5,940
kWh
|
$130
-
kW-mo/yr
|
- | - | $114 | |
06 | 2.7135: Install occupancy sensors | $1,428 | $2,892 |
$1,428
22,703
kWh
|
- | - | - | - | |
07 | 2.7232: Replace existing hvac unit with high efficiency model | $4,341 | $21,429 |
$3,792
60,291
kWh
|
$549
-
kW-mo/yr
|
- | - | - | |
TOTAL RECOMMENDED | $7,872 | $25,646 |
$6,603
104,979
kWh
|
$932
-
kW-mo/yr
|
$363
-
MMBtu
|
$(-100.0) | $74 | ||
TOTAL IMPLEMENTED | $6,823 | $24,771 |
$6,104
97,041
kWh
|
$745
-
kW-mo/yr
|
- | $(-100.0) | $74 | ||
Yearly Savings* | Imp'd Cost* | Electricity Usage Savings | Electricity Demand Savings | Natural Gas Savings | Personnel Changes Savings | Ancillary Material Cost Savings |
*Savings and costs are best estimates based on the center's site visit, associated engineering analysis, and typical capital and labor costs