Assessment Year | 2000 |
---|---|
Principal Product | Mirrors and glass |
NAICS |
n/a
|
SIC | 3231: Glass Products, Made of Purchased Glass |
Sales Range | $10 M to 50M |
# of Employees | 260 |
Plant Area |
175,000
ft2
|
Annual Production | 19,000
thousand feet
|
Production Hrs. Annual | 4,000
hrs
|
Location (State) | North Carolina |
Facility Energy Cost and Usage
Source | Yearly Cost | Usage | Unit Cost | |
---|---|---|---|---|
Electricity Usage | $134,619 | 3,481,243 |
kWh
|
$0.039 |
Electricity Demand | $66,101 | 14,064 |
kW-mo/yr
|
$4.70 |
Electricity Fees | $2,312 | - |
|
- |
Fuel Oil #4 | $26,720 | 9,990 |
MMBtu
|
$2.67 |
TOTAL YEARLY COSTS | - | |||
RECOMMENDED SAVINGS* | $157,268 |
See individual recommendations below
*Non-energy impacts included in savings.
|
||
IMPLEMENTED SAVINGS* | $11,686 |
Recommendations
# | Description | Yearly Savings* | Imp'd Cost* | Status | Electricity Usage Savings | Electricity Demand Savings | Fuel Oil #4 Savings | Water Disposal Savings | Solid Waste (non-haz) Savings | Administrative Changes Savings | Water Consumption Savings | Increase in Production Savings |
---|---|---|---|---|---|---|---|---|---|---|---|---|
01 | 2.1133: Adjust burners for efficient operation | $637 | $800 | - | - |
$637
-
MMBtu
|
- | - | - | - | - | |
02 | 2.2437: Recover waste heat from equipment | $537 | $1,700 | - | - |
$537
-
MMBtu
|
- | - | - | - | - | |
03 | 2.7122: Disconnect ballasts | $441 | $500 |
$328
7,913
kWh
|
$113
-
kW-mo/yr
|
- | - | - | - | - | - | |
04 | 2.7142: Utilize higher efficiency lamps and/or ballasts | $1,808 | $4,950 |
$545
13,189
kWh
|
$297
-
kW-mo/yr
|
- | - | - | $966 | - | - | |
05 | 2.2515: Use optimum thickness insulation | $4,274 | $1,200 |
$3,180
77,667
kWh
|
$1,094
-
kW-mo/yr
|
- | - | - | - | - | - | |
06 | 2.4231: Reduce the pressure of compressed air to the minimum required | $1,584 | $50 |
$1,584
38,687
kWh
|
- | - | - | - | - | - | - | |
07 | 3.4156: Use flow control valves on equipment to optimize water use | $112 | $90 | - | - | - | - | - | - |
$112
-
Tgal
|
- | |
08 | 3.5313: Increase amount of waste recovered for resale | $4,750 | $1,000 | - | - | - | - |
$4,750
-
lb
|
- | - | - | |
09 | 4.424: Improve space comfort conditioning | $143,125 | $27,000 | - | - | - |
$(-200.0)
-
Tgal
|
- | - | - | $143,325 | |
TOTAL RECOMMENDED | $157,268 | $37,290 |
$5,637
137,456
kWh
|
$1,504
-
kW-mo/yr
|
$1,174
-
MMBtu
|
$(-200.0)
-
Tgal
|
$4,750
-
lb
|
$966 |
$112
-
Tgal
|
$143,325 | ||
TOTAL IMPLEMENTED | $11,686 | $3,550 |
$5,092
124,267
kWh
|
$1,207
-
kW-mo/yr
|
$637
-
MMBtu
|
- |
$4,750
-
lb
|
- | - | - | ||
Yearly Savings* | Imp'd Cost* | Electricity Usage Savings | Electricity Demand Savings | Fuel Oil #4 Savings | Water Disposal Savings | Solid Waste (non-haz) Savings | Administrative Changes Savings | Water Consumption Savings | Increase in Production Savings |
*Savings and costs are best estimates based on the center's site visit, associated engineering analysis, and typical capital and labor costs