Assessment Year | 2002 |
---|---|
Principal Product | Tail Sections |
NAICS |
n/a
|
SIC | 3721: Aircraft |
Sales Range | $5 M to 10M |
# of Employees | 120 |
Plant Area |
100,000
ft2
|
Annual Production | 12
pieces
|
Production Hrs. Annual | 2,000
hrs
|
Location (State) | Mississippi |
View Case Study |
Facility Energy Cost and Usage
Source | Yearly Cost | Usage | Unit Cost | |
---|---|---|---|---|
Electricity Usage | $24,995 | 2,010,000 |
kWh
|
$0.012 |
Electricity Demand | $52,203 | 9,762 |
kW-mo/yr
|
$5.35 |
Electricity Fees | $63,686 | - |
|
- |
Natural Gas | $17,024 | 2,378 |
MMBtu
|
$7.16 |
TOTAL YEARLY COSTS | - | |||
RECOMMENDED SAVINGS* | $32,838 |
See individual recommendations below
*Non-energy impacts included in savings.
|
||
IMPLEMENTED SAVINGS* | $29,982 |
Recommendations
# | Description | Yearly Savings* | Imp'd Cost* | Status | Electricity Usage Savings | Electricity Demand Savings | Electricity Fees Savings | Natural Gas Savings | Administrative Changes Savings | Ancillary Material Cost Savings |
---|---|---|---|---|---|---|---|---|---|---|
01 | 2.1223: Install smaller boiler (increase high fire duty cycle) | $1,698 | $1,707 |
$89
2,638
kWh
|
- | $1 |
$1,608
-
MMBtu
|
- | - | |
02 | 2.4314: Use synthetic lubricant | $1,158 | $760 |
$470
13,988
kWh
|
$566
-
kW-mo/yr
|
$15 | - | - | $107 | |
03 | 2.4236: Eliminate leaks in inert gas and compressed air lines/ valves | $982 | $477 |
$967
28,775
kWh
|
- | $15 | - | - | - | |
04 | 4.652: Replace existing equipment with more suitable substitutes | $29,000 | $79,245 | - | - | - | - | $29,000 | - | |
TOTAL RECOMMENDED | $32,838 | $82,189 |
$1,526
45,401
kWh
|
$566
-
kW-mo/yr
|
$31 |
$1,608
-
MMBtu
|
$29,000 | $107 | ||
TOTAL IMPLEMENTED | $29,982 | $79,722 |
$967
28,775
kWh
|
- | $15 | - | $29,000 | - |
*Savings and costs are best estimates based on the center's site visit, associated engineering analysis, and typical capital and labor costs