| Assessment Year | 2006 | 
|---|---|
| Principal Product | Glass | 
| NAICS | 327215: Glass Product Manufacturing Made of Purchased Glass | 
| SIC | 3231: Glass Products, Made of Purchased Glass | 
| Sales Range | $5 Mto 10 M | 
| # of Employees | 115 | 
| Plant Area | 100,000 
ft2
 | 
| Annual Production | 4,000 
thousand feet
 | 
| Production Hrs. Annual | 5,000 
hrs
 | 
| Location (State) | Florida | 
Facility Energy Cost and Usage
| Source | Yearly Cost | Usage | Unit Cost | |
|---|---|---|---|---|
| Electricity Usage | $217,088 | 4,007,948 | 
kWh
 | $0.054 | 
| Electricity Demand | $83,445 | 12,838 | 
kW-mo/yr
 | $6.50 | 
| Electricity Fees | $27,052 | - |  | - | 
| TOTAL YEARLY COSTS | - | |||
| RECOMMENDED SAVINGS* | $50,586 | See individual recommendations below*Non-energy impacts included in savings. | ||
| IMPLEMENTED SAVINGS* | $44,032 | |||
Recommendations
| # | Description | Yearly Savings* | Imp'd Cost* | Status | Electricity Usage Savings | Electricity Demand Savings | Administrative Changes Savings | 
|---|---|---|---|---|---|---|---|
| 01 | 2.4146: Use adjustable frequency drive or multiple speed motors on existing system | $36,851 | $40,224 | $35,115 641,128
                                 
kWh
 | $1,736 -
                                 
kW-mo/yr
 | - | |
| 02 | 2.7111: Reduce illumination to minimum necessary levels | $4,544 | $146 | $4,443 81,120
                                 
kWh
 | $101 -
                                 
kW-mo/yr
 | - | |
| 03 | 2.4236: Eliminate leaks in inert gas and compressed air lines/ valves | $3,741 | $1,074 | $3,134 57,213
                                 
kWh
 | $607 -
                                 
kW-mo/yr
 | - | |
| 04 | 2.4231: Reduce the pressure of compressed air to the minimum required | $2,010 | $2,506 | $1,587 28,971
                                 
kWh
 | $423 -
                                 
kW-mo/yr
 | - | |
| 05 | 2.4111: Utilize energy-efficient belts and other improved mechanisms | $1,760 | - | $1,370 24,986
                                 
kWh
 | $390 -
                                 
kW-mo/yr
 | - | |
| 06 | 2.8114: Change rate schedules or other changes in utility service | $1,680 | $100 | - | - | $1,680 | |
| TOTAL RECOMMENDED | $50,586 | $44,050 | $45,649 833,418
                                 
kWh
 | $3,257 -
                                 
kW-mo/yr
 | $1,680 | ||
| TOTAL IMPLEMENTED | $44,032 | $41,398 | $39,619 723,327
                                 
kWh
 | $2,733 -
                                 
kW-mo/yr
 | $1,680 | ||
| Yearly Savings* | Imp'd Cost* | Electricity Usage Savings | Electricity Demand Savings | Administrative Changes Savings | |||
*Savings and costs are best estimates based on the center's site visit, associated engineering analysis, and typical capital and labor costs
             
             
             
            