Assessment Year | 2012 |
---|---|
Principal Product | Rubber Shaft Seals |
NAICS | 339991: Gasket, Packing, and Sealing Device Manufacturing |
SIC | 3053: Gaskets, Packing, and Sealing Devices |
Sales Range | $50 M to 100M |
# of Employees | 409 |
Plant Area |
290,000
ft2
|
Annual Production | 365,000,000
pieces
|
Production Hrs. Annual | 6,240
hrs
|
Location (State) | New Hampshire |
Facility Energy Cost and Usage
Source | Yearly Cost | Usage | Unit Cost | |
---|---|---|---|---|
Electricity Usage | $1,361,923 | 15,704,834 |
kWh
|
$0.087 |
Electricity Demand | $333,063 | 33,311 |
kW-mo/yr
|
$10.00 |
Fuel Oil #6 | $685,242 | 44,116 |
MMBtu
|
$15.53 |
Other Gas | $281,188 | 16,131 |
MMBtu
|
$17.43 |
TOTAL YEARLY COSTS | - | |||
RECOMMENDED SAVINGS* | $173,139 |
See individual recommendations below
*Non-energy impacts included in savings.
|
||
IMPLEMENTED SAVINGS* | $16,550 |
Recommendations
# | Description | Yearly Savings* | Imp'd Cost* | Status | Electricity Usage Savings | Electricity Demand Savings | Fuel Oil #6 Savings | Administrative Changes Savings |
---|---|---|---|---|---|---|---|---|
01 | 2.2437: Recover waste heat from equipment | $99,334 | $216,000 |
$(-29,800.0)
(-345,310)
kWh
|
$(-4,900.0)
-
kW-mo/yr
|
$134,034
-
MMBtu
|
- | |
02 | 2.6212: Turn off equipment during breaks, reduce operating time | $36,978 | $9,000 |
$36,978
428,480
kWh
|
- | - | - | |
03 | 2.4322: Use or replace with energy efficient substitutes | $18,123 | $77,100 |
$3,123
36,192
kWh
|
- | - | $15,000 | |
04 | 2.4231: Reduce the pressure of compressed air to the minimum required | $8,077 | $8,000 |
$8,077
93,600
kWh
|
- | - | - | |
05 | 2.6242: Minimize operation of equipment maintained in standby condition | $4,883 | $3,120 |
$4,883
56,576
kWh
|
- | - | - | |
06 | 2.6242: Minimize operation of equipment maintained in standby condition | $3,590 | $3,120 |
$3,590
41,600
kWh
|
- | - | - | |
07 | 2.6212: Turn off equipment during breaks, reduce operating time | $2,154 | $2,000 |
$2,154
24,960
kWh
|
- | - | - | |
TOTAL RECOMMENDED | $173,139 | $318,340 |
$29,005
336,098
kWh
|
$(-4,900.0)
-
kW-mo/yr
|
$134,034
-
MMBtu
|
$15,000 | ||
TOTAL IMPLEMENTED | $16,550 | $14,240 |
$16,550
191,776
kWh
|
- | - | - | ||
Yearly Savings* | Imp'd Cost* | Electricity Usage Savings | Electricity Demand Savings | Fuel Oil #6 Savings | Administrative Changes Savings |
*Savings and costs are best estimates based on the center's site visit, associated engineering analysis, and typical capital and labor costs