ITAC Assessment: MA0826
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ITAC Assessment: MA0826
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Assessment Year 2021
Principal Product Printed circuit boards
NAICS 334412: Bare Printed Circuit Board Manufacturing
SIC 3672: Printed Circuit Boards
Sales Range $1
M
to 5
M
# of Employees 20
Plant Area 27,000
ft2
Annual Production 50,400
lb
Production Hrs. Annual 2,185
hrs
Location (State) New Hampshire

Facility Energy Cost and Usage

Source Yearly Cost Usage
Electricity Usage $121,861 1,078,800
kWh
Electricity Demand $70,282 5,294
kW-mo/yr
Electricity Fees $5,151 -
Natural Gas $5,490 377
MMBtu
Waste Disposal Costs
Water Usage $25,861 3,866
Tgal
Water Disposal $17,229 3,866
Tgal
TOTAL YEARLY COSTS $245,873
RECOMMENDED SAVINGS* $37,374 *Non-energy impacts included in savings.
IMPLEMENTED SAVINGS* $1,530

Recommendations

# Description Yearly Savings* Imp'd Cost* Status Electricity Usage Savings Electricity Demand Savings Water Usage Savings Ancillary Material Cost Savings
01 3.3122: Use filtration, centrifuging to remove contaminants $27,883 $250,000 $(-2,725.0)
(-24,119)
kWh
$(-996.0)
-
kW-mo/yr
$24,774
-
Tgal
$6,830
02 2.4146: Use adjustable frequency drive or multiple speed motors on existing system $4,639 $14,650 $4,639
41,053
kWh
- - -
03 2.2614: Use cooling tower or economizer to replace chiller cooling $2,447 $10,800 $1,332
11,791
kWh
$1,115
-
kW-mo/yr
- -
04 2.4146: Use adjustable frequency drive or multiple speed motors on existing system $979 $1,631 $979
8,664
kWh
- - -
05 2.6218: Turn off equipment when not in use $552 $250 $552
4,881
kWh
- - -
06 2.4236: Eliminate leaks in inert gas and compressed air lines/ valves $551 $1,450 $551
4,877
kWh
- - -
07 2.4239: Eliminate or reduce compressed air usage $323 $625 $323
2,859
kWh
- - -
TOTAL RECOMMENDED $37,374 $279,406 $5,651
50,006
kWh
$119
-
kW-mo/yr
$24,774
-
Tgal
$6,830
TOTAL IMPLEMENTED $1,530 $3,081 $1,530
13,541
kWh
- - -
Yearly Savings* Imp'd Cost* Electricity Usage Savings Electricity Demand Savings Water Usage Savings Ancillary Material Cost Savings
*Savings and costs are best estimates based on the center's site visit, associated engineering analysis, and typical capital and labor costs