ITAC Assessment: MA0721
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ITAC Assessment: MA0721
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Assessment Year 2013
Principal Product Rpair of Helicopter Parts
NAICS 336413: Other Aircraft Parts and Auxiliary Equipment Manufacturing
SIC 3728: Aircraft Parts and Auxiliary Equipment, Not Elsewhere Classified
Sales Range $50
M
to 100
M
# of Employees 200
Plant Area 180,000
ft2
Annual Production 4,560
pieces
Production Hrs. Annual 5,406
hrs
Location (State) Connecticut

Facility Energy Cost and Usage

Source Yearly Cost Usage
Electricity Usage $333,834 2,764,400
kWh
Electricity Demand $102,784 7,380
kW-mo/yr
Electricity Fees $4,116 -
Natural Gas $88,481 6,104
MMBtu
TOTAL YEARLY COSTS -
RECOMMENDED SAVINGS* $49,273 *Non-energy impacts included in savings.
IMPLEMENTED SAVINGS* $30,225

Recommendations

# Description Yearly Savings* Imp'd Cost* Status Electricity Usage Savings Natural Gas Savings Administrative Changes Savings
01 2.8114: Change rate schedules or other changes in utility service $15,477 $1,400 - - $15,477
02 2.7224: Reduce space conditioning during non-working hours $10,906 $7,500 $6,773
56,918
kWh
$4,133
-
MMBtu
-
03 2.7111: Reduce illumination to minimum necessary levels $7,493 $11,000 $7,493
60,916
kWh
- -
04 2.8121: Apply for tax-free status for energy purchases $4,864 $200 - - $4,864
05 2.7221: Lower temperature during the winter season and vice-versa $2,474 $200 $1,143
9,603
kWh
$1,331
-
MMBtu
-
06 2.2135: Repair and eliminate steam leaks $2,358 $1,120 $2,358
19,167
kWh
- -
07 2.4231: Reduce the pressure of compressed air to the minimum required $2,130 $1,020 $2,130
17,313
kWh
- -
08 2.4146: Use adjustable frequency drive or multiple speed motors on existing system $2,106 $6,390 $2,106
17,118
kWh
- -
09 2.2136: Install / repair insulation on steam lines $1,465 $1,650 - $1,465
-
MMBtu
-
TOTAL RECOMMENDED $49,273 $30,480 $22,003
181,035
kWh
$6,929
-
MMBtu
$20,341
TOTAL IMPLEMENTED $30,225 $21,040 $19,897
163,917
kWh
$5,464
-
MMBtu
$4,864
Yearly Savings* Imp'd Cost* Electricity Usage Savings Natural Gas Savings Administrative Changes Savings
*Savings and costs are best estimates based on the center's site visit, associated engineering analysis, and typical capital and labor costs