| Assessment Year | 1992 |
|---|---|
| Principal Product | INVESTMENT CASTINGS |
| NAICS |
n/a
|
| SIC | 3324: Steel Investment Foundries |
| Sales Range | $10 M to 50M |
| # of Employees | 500 |
| Plant Area |
n/a
|
| Annual Production | 7,000,000
lb
|
| Production Hrs. Annual | 6,120
hrs
|
| Location (State) | New Hampshire |
Facility Energy Cost and Usage
| Source | Yearly Cost | Usage | Unit Cost | |
|---|---|---|---|---|
| Electricity Usage | $1,336,182 | 18,333,822 |
kWh
|
$0.073 |
| LPG | $555,181 | 109,365 |
MMBtu
|
$5.08 |
| TOTAL YEARLY COSTS | - | |||
| RECOMMENDED SAVINGS* | $101,259 |
See individual recommendations below
*Non-energy impacts included in savings.
|
||
| IMPLEMENTED SAVINGS* | $8,244 | |||
Recommendations
| # | Description | Yearly Savings* | Imp'd Cost* | Status | Electricity Usage Savings | LPG Savings | Administrative Changes Savings |
|---|---|---|---|---|---|---|---|
| 01 | 2.2443: Re-use or recycle hot or cold process exhaust air | $31,842 | $90,600 |
$(-8,224.0)
(-113,130)
kWh
|
$40,066
-
MMBtu
|
- | |
| 02 | 2.4322: Use or replace with energy efficient substitutes | $61,173 | $70,000 | - |
$61,173
-
MMBtu
|
- | |
| 03 | 2.2113: Repair or replace steam traps | $2,293 | $2 | - |
$3,231
-
MMBtu
|
$(-938.0) | |
| 04 | 2.7316: Centralize control of exhaust fans to ensure their shutdown, or establish program to ensure manual shutdown | $5,067 | - |
$983
13,482
kWh
|
$4,084
-
MMBtu
|
- | |
| 05 | 2.2121: Increase amount of condensate returned | $884 | $150 | - |
$884
-
MMBtu
|
- | |
| TOTAL RECOMMENDED | $101,259 | $160,752 |
$(-7,241.0)
(-99,648)
kWh
|
$109,438
-
MMBtu
|
$(-938.0) | ||
| TOTAL IMPLEMENTED | $8,244 | $152 |
$983
13,482
kWh
|
$8,199
-
MMBtu
|
$(-938.0) | ||
*Savings and costs are best estimates based on the center's site visit, associated engineering analysis, and typical capital and labor costs