Assessment Year | 1999 |
---|---|
Principal Product | wood windows |
NAICS |
n/a
|
SIC | 2431: Millwork |
Sales Range | $10 M to 50M |
# of Employees | 100 |
Plant Area |
140,800
ft2
|
Annual Production | 47,500
pieces
|
Production Hrs. Annual | 2,100
hrs
|
Location (State) | Nebraska |
Facility Energy Cost and Usage
Source | Yearly Cost | Usage | Unit Cost | |
---|---|---|---|---|
Electricity Usage | $30,758 | 1,070,926 |
kWh
|
$0.029 |
Electricity Demand | $36,814 | 4,826 |
kW-mo/yr
|
$7.63 |
Natural Gas | $29,584 | 6,383 |
MMBtu
|
$4.63 |
TOTAL YEARLY COSTS | - | |||
RECOMMENDED SAVINGS* | $75,110 |
See individual recommendations below
*Non-energy impacts included in savings.
|
||
IMPLEMENTED SAVINGS* | - |
Recommendations
# | Description | Yearly Savings* | Imp'd Cost* | Status | Electricity Usage Savings | Electricity Demand Savings | Natural Gas Savings | Personnel Changes Savings | Primary Product Savings |
---|---|---|---|---|---|---|---|---|---|
01 | 2.6212: Turn off equipment during breaks, reduce operating time | $6,910 | $8,800 | n/a |
$1,980
86,166
kWh
|
$4,930
-
kW-mo/yr
|
- | - | - |
02 | 2.4236: Eliminate leaks in inert gas and compressed air lines/ valves | $900 | $520 | n/a |
$290
12,603
kWh
|
$610
-
kW-mo/yr
|
- | - | - |
03 | 2.2437: Recover waste heat from equipment | $620 | $730 | n/a | - | - |
$620
-
MMBtu
|
- | - |
04 | 4.513: Re-arrange equipment layout to reduce labor costs | $55,080 | $1,380 | n/a | - | - | - | $55,080 | - |
05 | 4.424: Improve space comfort conditioning | $11,600 | $10,670 | n/a | - | - | - | - | $11,600 |
TOTAL RECOMMENDED | $75,110 | $22,100 |
$2,270
98,769
kWh
|
$5,540
-
kW-mo/yr
|
$620
-
MMBtu
|
$55,080 | $11,600 | ||
TOTAL IMPLEMENTED | - | - | - | - | - | - | - |
*Savings and costs are best estimates based on the center's site visit, associated engineering analysis, and typical capital and labor costs