ITAC Assessment: KU0299
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ITAC Assessment: KU0299
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Assessment Year 1989
Principal Product DENIM JEANS
NAICS
n/a
SIC 2325: Men's and Boys' Separate Trousers and Slacks
Sales Range $50
M
to 100
M
# of Employees 265
Plant Area
n/a
Annual Production 1,900,000
pieces
Production Hrs. Annual 5,400
hrs
Location (State) Missouri

Facility Energy Cost and Usage

Source Yearly Cost Usage
Electricity Usage $100,913 1,785,756
kWh
Natural Gas $78,372 21,012
MMBtu
TOTAL YEARLY COSTS -
RECOMMENDED SAVINGS* $14,683 *Non-energy impacts included in savings.
IMPLEMENTED SAVINGS* $9,514

Recommendations

# Description Yearly Savings* Imp'd Cost* Status Electricity Usage Savings Natural Gas Savings Administrative Changes Savings
01 2.7142: Utilize higher efficiency lamps and/or ballasts $421 $121 $421
7,327
kWh
- -
02 2.7111: Reduce illumination to minimum necessary levels $447 $250 $447
7,913
kWh
- -
03 2.6212: Turn off equipment during breaks, reduce operating time $315 $150 $315
5,569
kWh
- -
04 2.2113: Repair or replace steam traps $8,388 $450 - $8,388
-
MMBtu
-
05 2.2437: Recover waste heat from equipment $3,205 $2,400 - $3,205
-
MMBtu
-
06 2.1123: Install automatic stack damper $1,466 $1,700 - $1,466
-
MMBtu
-
07 2.6214: Shut off pilots in standby equipment $258 - - $418
-
MMBtu
$(-160.0)
08 2.2511: Insulate bare equipment $183 $280 $75
1,465
kWh
$108
-
MMBtu
-
TOTAL RECOMMENDED $14,683 $5,351 $1,258
22,274
kWh
$13,585
-
MMBtu
$(-160.0)
TOTAL IMPLEMENTED $9,514 $821 $868
15,240
kWh
$8,806
-
MMBtu
$(-160.0)
Yearly Savings* Imp'd Cost* Electricity Usage Savings Natural Gas Savings Administrative Changes Savings
*Savings and costs are best estimates based on the center's site visit, associated engineering analysis, and typical capital and labor costs