| Assessment Year | 1989 |
|---|---|
| Principal Product | PRINTED LABELS |
| NAICS |
n/a
|
| SIC | 2759: Commercial Printing, Not Elsewhere Classified |
| Sales Range | $10 M to 50M |
| # of Employees | 155 |
| Plant Area |
n/a
|
| Annual Production | 0
units
|
| Production Hrs. Annual | 7,200
hrs
|
| Location (State) | Nebraska |
Facility Energy Cost and Usage
| Source | Yearly Cost | Usage | Unit Cost | |
|---|---|---|---|---|
| Electricity Usage | $76,282 | 1,601,993 |
kWh
|
$0.048 |
| Natural Gas | $13,132 | 3,401 |
MMBtu
|
$3.86 |
| TOTAL YEARLY COSTS | - | |||
| RECOMMENDED SAVINGS* | $18,114 |
See individual recommendations below
*Non-energy impacts included in savings.
|
||
| IMPLEMENTED SAVINGS* | $886 | |||
Recommendations
| # | Description | Yearly Savings* | Imp'd Cost* | Status | Electricity Usage Savings | Natural Gas Savings | Administrative Changes Savings |
|---|---|---|---|---|---|---|---|
| 01 | 2.2437: Recover waste heat from equipment | $935 | $462 |
$240
4,982
kWh
|
$695
-
MMBtu
|
- | |
| 02 | 2.7142: Utilize higher efficiency lamps and/or ballasts | $1,133 | $1,133 |
$1,133
23,740
kWh
|
- | - | |
| 03 | 2.4111: Utilize energy-efficient belts and other improved mechanisms | $187 | - |
$187
3,810
kWh
|
- | - | |
| 04 | 2.4312: Improve lubrication practices | $167 | - |
$167
3,517
kWh
|
- | - | |
| 05 | 2.6218: Turn off equipment when not in use | $291 | $350 |
$291
6,155
kWh
|
- | - | |
| 06 | 2.7226: Use computer programs to optimize hvac performance | $1,986 | $4,440 |
$1,986
41,618
kWh
|
- | - | |
| 07 | 3.4156: Use flow control valves on equipment to optimize water use | $318 | - | - | - | $318 | |
| 08 | 2.5194: Redesign process | $11,461 | $13,200 |
$9,025
189,625
kWh
|
- | $2,436 | |
| 09 | 2.6121: Reduce hot water temperature to the minimum required | $241 | - |
$192
4,103
kWh
|
$49
-
MMBtu
|
- | |
| 10 | 2.7243: Improve air circulation with destratification fans / other methods | $1,395 | $2,300 |
$1,395
29,308
kWh
|
- | - | |
| TOTAL RECOMMENDED | $18,114 | $21,885 |
$14,616
306,858
kWh
|
$744
-
MMBtu
|
$2,754 | ||
| TOTAL IMPLEMENTED | $886 | $350 |
$837
17,585
kWh
|
$49
-
MMBtu
|
- | ||
| Yearly Savings* | Imp'd Cost* | Electricity Usage Savings | Natural Gas Savings | Administrative Changes Savings | |||
*Savings and costs are best estimates based on the center's site visit, associated engineering analysis, and typical capital and labor costs