ITAC Assessment: KU0199
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ITAC Assessment: KU0199
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Assessment Year 1986
Principal Product TRUCK BODIES & TRAILERS
NAICS
n/a
SIC 3713: Truck and Bus Bodies
Sales Range $10
M
to 50
M
# of Employees 70
Plant Area
n/a
Annual Production 650
pieces
Production Hrs. Annual 0
hrs
Location (State) Missouri

Facility Energy Cost and Usage

Source Yearly Cost Usage
Electricity Usage $64,095 739,156
kWh
Natural Gas $24,587 5,508
MMBtu
TOTAL YEARLY COSTS -
RECOMMENDED SAVINGS* $17,560 *Non-energy impacts included in savings.
IMPLEMENTED SAVINGS* $13,044

Recommendations

# Description Yearly Savings* Imp'd Cost* Status Electricity Usage Savings Natural Gas Savings Administrative Changes Savings
01 2.7142: Utilize higher efficiency lamps and/or ballasts $8,919 $6,173 $8,919
102,872
kWh
- -
02 2.1311: Replace electrically-operated equipment with fossil fuel equipment $4,324 $6,000 $5,539
63,892
kWh
$(-1,215.0)
-
MMBtu
-
03 2.7221: Lower temperature during the winter season and vice-versa $1,330 $100 $1,330
15,240
kWh
- -
04 2.7221: Lower temperature during the winter season and vice-versa $1,289 $100 - $1,289
-
MMBtu
-
05 2.7221: Lower temperature during the winter season and vice-versa $906 $34 $152
1,758
kWh
$754
-
MMBtu
-
06 2.4236: Eliminate leaks in inert gas and compressed air lines/ valves $600 $200 $600
7,034
kWh
- -
07 2.1232: Keep boiler tubes clean $112 $100 - $162
-
MMBtu
$(-50.0)
08 2.1233: Analyze flue gas for proper air/fuel ratio $80 - - $130
-
MMBtu
$(-50.0)
TOTAL RECOMMENDED $17,560 $12,707 $16,540
190,796
kWh
$1,120
-
MMBtu
$(-100.0)
TOTAL IMPLEMENTED $13,044 $6,607 $11,001
126,904
kWh
$2,043
-
MMBtu
-
Yearly Savings* Imp'd Cost* Electricity Usage Savings Natural Gas Savings Administrative Changes Savings
*Savings and costs are best estimates based on the center's site visit, associated engineering analysis, and typical capital and labor costs