| Assessment Year | 1985 |
|---|---|
| Principal Product | ENGINE GENERATOR ASSEMBLY |
| NAICS |
n/a
|
| SIC | 3621: Motors and Generators |
| Sales Range | $10 M to 50M |
| # of Employees | 62 |
| Plant Area |
n/a
|
| Annual Production | 5,000
pieces
|
| Production Hrs. Annual | 2,125
hrs
|
| Location (State) | Kansas |
Facility Energy Cost and Usage
| Source | Yearly Cost | Usage | Unit Cost | |
|---|---|---|---|---|
| Electricity Usage | $25,995 | 404,748 |
kWh
|
$0.064 |
| Natural Gas | $19,095 | 4,636 |
MMBtu
|
$4.12 |
| TOTAL YEARLY COSTS | - | |||
| RECOMMENDED SAVINGS* | $4,030 |
See individual recommendations below
*Non-energy impacts included in savings.
|
||
| IMPLEMENTED SAVINGS* | $1,953 | |||
Recommendations
| # | Description | Yearly Savings* | Imp'd Cost* | Status | Electricity Usage Savings | Natural Gas Savings | Administrative Changes Savings |
|---|---|---|---|---|---|---|---|
| 01 | 2.1123: Install automatic stack damper | $1,232 | $1,875 | - |
$1,232
-
MMBtu
|
- | |
| 02 | 2.7142: Utilize higher efficiency lamps and/or ballasts | $1,562 | $1,540 |
$1,562
24,326
kWh
|
- | - | |
| 03 | 2.1233: Analyze flue gas for proper air/fuel ratio | $618 | $1,200 | - |
$618
-
MMBtu
|
- | |
| 04 | 2.7314: Reduce ventilation air | $227 | $200 | - |
$227
-
MMBtu
|
- | |
| 05 | 2.6214: Shut off pilots in standby equipment | $203 | - | - |
$453
-
MMBtu
|
$(-250.0) | |
| 06 | 2.4236: Eliminate leaks in inert gas and compressed air lines/ valves | $188 | $60 |
$188
2,931
kWh
|
- | - | |
| TOTAL RECOMMENDED | $4,030 | $4,875 |
$1,750
27,257
kWh
|
$2,530
-
MMBtu
|
$(-250.0) | ||
| TOTAL IMPLEMENTED | $1,953 | $1,600 |
$1,750
27,257
kWh
|
$453
-
MMBtu
|
$(-250.0) | ||
| Yearly Savings* | Imp'd Cost* | Electricity Usage Savings | Natural Gas Savings | Administrative Changes Savings | |||
*Savings and costs are best estimates based on the center's site visit, associated engineering analysis, and typical capital and labor costs