Assessment Year | 1985 |
---|---|
Principal Product | ENGINE GENERATOR ASSEMBLY |
NAICS |
n/a
|
SIC | 3621: Motors and Generators |
Sales Range | $10 M to 50M |
# of Employees | 62 |
Plant Area |
n/a
|
Annual Production | 5,000
pieces
|
Production Hrs. Annual | 2,125
hrs
|
Location (State) | Kansas |
Facility Energy Cost and Usage
Source | Yearly Cost | Usage | Unit Cost | |
---|---|---|---|---|
Electricity Usage | $25,995 | 404,748 |
kWh
|
$0.064 |
Natural Gas | $19,095 | 4,636 |
MMBtu
|
$4.12 |
TOTAL YEARLY COSTS | - | |||
RECOMMENDED SAVINGS* | $4,030 |
See individual recommendations below
*Non-energy impacts included in savings.
|
||
IMPLEMENTED SAVINGS* | $1,953 |
Recommendations
# | Description | Yearly Savings* | Imp'd Cost* | Status | Electricity Usage Savings | Natural Gas Savings | Administrative Changes Savings |
---|---|---|---|---|---|---|---|
01 | 2.1123: Install automatic stack damper | $1,232 | $1,875 | - |
$1,232
-
MMBtu
|
- | |
02 | 2.7142: Utilize higher efficiency lamps and/or ballasts | $1,562 | $1,540 |
$1,562
24,326
kWh
|
- | - | |
03 | 2.1233: Analyze flue gas for proper air/fuel ratio | $618 | $1,200 | - |
$618
-
MMBtu
|
- | |
04 | 2.7314: Reduce ventilation air | $227 | $200 | - |
$227
-
MMBtu
|
- | |
05 | 2.6214: Shut off pilots in standby equipment | $203 | - | - |
$453
-
MMBtu
|
$(-250.0) | |
06 | 2.4236: Eliminate leaks in inert gas and compressed air lines/ valves | $188 | $60 |
$188
2,931
kWh
|
- | - | |
TOTAL RECOMMENDED | $4,030 | $4,875 |
$1,750
27,257
kWh
|
$2,530
-
MMBtu
|
$(-250.0) | ||
TOTAL IMPLEMENTED | $1,953 | $1,600 |
$1,750
27,257
kWh
|
$453
-
MMBtu
|
$(-250.0) | ||
Yearly Savings* | Imp'd Cost* | Electricity Usage Savings | Natural Gas Savings | Administrative Changes Savings |
*Savings and costs are best estimates based on the center's site visit, associated engineering analysis, and typical capital and labor costs