| Assessment Year | 2023 |
|---|---|
| Principal Product | Resilient Flooring |
| NAICS | 326199: All Other Plastics Product Manufacturing |
| SIC | 3996: Linoleum, Asphalted-Felt-Base, and Other Hard Surface Floor Coverings, Not Elsewhere Classified |
| Sales Range | $50 M to 100M |
| # of Employees | 167 |
| Plant Area |
129,000
ft2
|
| Annual Production | 65,000,000
units
|
| Production Hrs. Annual | 6,240
hrs
|
| Location (State) | Georgia |
Facility Energy Cost and Usage
| Source | Yearly Cost | Usage | Unit Cost | ||
|---|---|---|---|---|---|
| Electricity Usage | $1,212,491 | 15,661,652 |
kWh
|
$0.077 | |
| Natural Gas | $675,170 | 55,159 |
MMBtu
|
$12.24 | |
| Waste Disposal Costs | |||||
| Water Usage | $17,610 | 2,620 |
Tgal
|
$6.72 | |
| Water Disposal | $16,561 | 2,620 |
Tgal
|
$6.32 | |
| TOTAL YEARLY COSTS | $1,921,832 | ||||
| RECOMMENDED SAVINGS* | $175,330 |
See individual recommendations below
*Non-energy impacts included in savings.
|
|||
| IMPLEMENTED SAVINGS* | $12,574 | ||||
Recommendations
| # | Description | Yearly Savings* | Imp'd Cost* | Status | Electricity Usage Savings | Natural Gas Savings | Personnel Changes Savings | Administrative Changes Savings |
|---|---|---|---|---|---|---|---|---|
| 01 | 2.4236: Eliminate leaks in inert gas and compressed air lines/ valves | $12,574 | $6,440 |
$12,574
141,286
kWh
|
- | - | - | |
| 02 | 2.1131: Repair faulty insulation in furnaces, boilers, etc | $19,596 | $10,708 | - |
$19,596
-
MMBtu
|
- | - | |
| 03 | 2.2123: Insulate feedwater tank | $4,841 | $4,104 | - |
$4,841
-
MMBtu
|
- | - | |
| 04 | 2.2136: Install / repair insulation on steam lines | $13,819 | $3,753 | - |
$13,819
-
MMBtu
|
- | - | |
| 05 | 2.1233: Analyze flue gas for proper air/fuel ratio | $1,129 | - | - |
$1,909
-
MMBtu
|
- | $(-780.0) | |
| 06 | 2.3417: Use waste heat with a closed-cycle gas turbine-generator set to cogenerate electricity and heat | $66,324 | $627,000 |
$111,072
1,248,000
kWh
|
$(-38,348.0)
-
MMBtu
|
$(-6,400.0) | - | |
| 07 | 2.9114: Use solar heat to make electricty | $57,047 | $422,421 |
$57,047
640,983
kWh
|
- | - | - | |
| TOTAL RECOMMENDED | $175,330 | $1,074,426 |
$180,693
2,030,269
kWh
|
$1,817
-
MMBtu
|
$(-6,400.0) | $(-780.0) | ||
| TOTAL IMPLEMENTED | $12,574 | $6,440 |
$12,574
141,286
kWh
|
- | - | - | ||
| Yearly Savings* | Imp'd Cost* | Electricity Usage Savings | Natural Gas Savings | Personnel Changes Savings | Administrative Changes Savings | |||
*Savings and costs are best estimates based on the center's site visit, associated engineering analysis, and typical capital and labor costs