ITAC Assessment: IA0447
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ITAC Assessment: IA0447
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Assessment Year 2010
Principal Product Fasteners
NAICS 336390: Other Motor Vehicle Parts Manufacturing
SIC 3069: Fabricated Rubber Products, Not Elsewhere Classified
Sales Range $50
M
to 100
M
# of Employees 129
Plant Area 150,000
ft2
Annual Production 11,000,000
lb
Production Hrs. Annual 8,760
hrs
Location (State) Minnesota

Facility Energy Cost and Usage

Source Yearly Cost Usage
Electricity Usage $301,496 6,908,725
kWh
Electricity Demand $180,804 13,908
kW-mo/yr
Natural Gas $139,741 21,020
MMBtu
TOTAL YEARLY COSTS -
RECOMMENDED SAVINGS* $60,539 *Non-energy impacts included in savings.
IMPLEMENTED SAVINGS* $52,993

Recommendations

# Description Yearly Savings* Imp'd Cost* Status Electricity Usage Savings Electricity Demand Savings Natural Gas Savings
01 2.7142: Utilize higher efficiency lamps and/or ballasts $745 $487 $511
11,650
kWh
$234
-
kW-mo/yr
-
02 2.7142: Utilize higher efficiency lamps and/or ballasts $17,514 $13,439 $12,460
283,824
kWh
$5,054
-
kW-mo/yr
-
03 2.4239: Eliminate or reduce compressed air usage $2,599 $1,140 $1,398
31,841
kWh
$1,201
-
kW-mo/yr
-
04 2.7314: Reduce ventilation air $3,072 $2,000 $3,072
69,989
kWh
- -
05 2.2692: Use outside cold water source as a supply of cooling water $6,801 $42,100 $6,801
154,926
kWh
- -
06 2.1224: Replace boiler $29,283 $53,900 $2,621
59,702
kWh
- $26,662
-
MMBtu
07 2.2191: Substitute hot process fluids for steam $525 $5,000 $(-1,902.0)
(-43,222)
kWh
- $2,427
-
MMBtu
TOTAL RECOMMENDED $60,539 $118,066 $24,961
568,710
kWh
$6,489
-
kW-mo/yr
$29,089
-
MMBtu
TOTAL IMPLEMENTED $52,993 $75,479 $17,649
402,134
kWh
$6,255
-
kW-mo/yr
$29,089
-
MMBtu
Yearly Savings* Imp'd Cost* Electricity Usage Savings Electricity Demand Savings Natural Gas Savings
*Savings and costs are best estimates based on the center's site visit, associated engineering analysis, and typical capital and labor costs