Assessment Year | 1994 |
---|---|
Principal Product | corrugated containers |
NAICS |
n/a
|
SIC | 2653: Corrugated and Solid Fiber Boxes |
Sales Range | $10 M to 50M |
# of Employees | 275 |
Plant Area |
184,000
ft2
|
Annual Production | 67,000
ton
|
Production Hrs. Annual | 8,112
hrs
|
Location (State) | Iowa |
Facility Energy Cost and Usage
Source | Yearly Cost | Usage | Unit Cost | |
---|---|---|---|---|
Electricity Usage | $351,782 | 8,619,871 |
kWh
|
$0.041 |
Natural Gas | $195,826 | 68,056 |
MMBtu
|
$2.88 |
TOTAL YEARLY COSTS | - | |||
RECOMMENDED SAVINGS* | $49,485 |
See individual recommendations below
*Non-energy impacts included in savings.
|
||
IMPLEMENTED SAVINGS* | $42,650 |
Recommendations
# | Description | Yearly Savings* | Imp'd Cost* | Status | Electricity Usage Savings | Natural Gas Savings |
---|---|---|---|---|---|---|
01 | 2.3212: Optimize plant power factor | $19,385 | $17,738 |
$19,385
-
kWh
|
- | |
02 | 2.4236: Eliminate leaks in inert gas and compressed air lines/ valves | $10,489 | $500 |
$10,489
257,034
kWh
|
- | |
03 | 2.4231: Reduce the pressure of compressed air to the minimum required | $6,257 | $50 |
$6,257
153,283
kWh
|
- | |
04 | 2.7142: Utilize higher efficiency lamps and/or ballasts | $7,368 | $1,803 |
$7,368
179,660
kWh
|
- | |
05 | 2.7135: Install occupancy sensors | $578 | $997 |
$578
14,068
kWh
|
- | |
06 | 2.1213: Direct warmest air to combustion intake | $4,490 | $12,600 | - |
$4,490
-
MMBtu
|
|
07 | 2.2122: Install / repair insulation on condensate lines | $918 | $373 | - |
$918
-
MMBtu
|
|
TOTAL RECOMMENDED | $49,485 | $34,061 |
$44,077
604,045
kWh
|
$5,408
-
MMBtu
|
||
TOTAL IMPLEMENTED | $42,650 | $33,014 |
$37,242
436,694
kWh
|
$5,408
-
MMBtu
|
||
Yearly Savings* | Imp'd Cost* | Electricity Usage Savings | Natural Gas Savings |
*Savings and costs are best estimates based on the center's site visit, associated engineering analysis, and typical capital and labor costs