ITAC Assessment: GT0827
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ITAC Assessment: GT0827
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Assessment Year 2006
Principal Product Chicken
NAICS 311615: Poultry Processing
SIC 2015: Poultry Slaughtering and Processing
Sales Range greater than $500
M
# of Employees 4,600
Plant Area 500,000
ft2
Annual Production 700,000,000
lb
Production Hrs. Annual 6,000
hrs
Location (State) Georgia

Facility Energy Cost and Usage

Source Yearly Cost Usage
Electricity Usage $1,886,786 31,284,464
kWh
Natural Gas $3,362,812 334,418
MMBtu
TOTAL YEARLY COSTS -
RECOMMENDED SAVINGS* $685,319 *Non-energy impacts included in savings.
IMPLEMENTED SAVINGS* $255,200

Recommendations

# Description Yearly Savings* Imp'd Cost* Status Electricity Usage Savings Natural Gas Savings Administrative Changes Savings Water Consumption Savings
01 2.4111: Utilize energy-efficient belts and other improved mechanisms $5,551 $1,487 $5,551
109,489
kWh
- - -
02 2.2414: Use waste heat from hot flue gases to preheat $325,944 $38,000 - $325,944
-
MMBtu
- -
03 2.2128: Use steam condensate for hot water supply (non-potable) $85,490 $12,500 - $85,490
-
MMBtu
- -
04 2.2162: Reduce excess steam bleeding $10,400 $39,900 - $9,909
-
MMBtu
- $491
-
Tgal
05 2.7142: Utilize higher efficiency lamps and/or ballasts $2,421 $4,053 $2,421
47,750
kWh
- - -
06 2.7142: Utilize higher efficiency lamps and/or ballasts $2,361 $2,328 $2,361
46,560
kWh
- - -
07 2.6242: Minimize operation of equipment maintained in standby condition $2,734 $3,500 $963
19,000
kWh
$1,771
-
MMBtu
- -
08 3.4155: Meter waste water $81,583 $5,250 - - $81,583 -
09 2.2437: Recover waste heat from equipment $158,948 $150,000 - $158,948
-
MMBtu
- -
10 2.4236: Eliminate leaks in inert gas and compressed air lines/ valves $9,887 $3,400 $9,887
195,000
kWh
- - -
TOTAL RECOMMENDED $685,319 $260,418 $21,183
417,799
kWh
$582,062
-
MMBtu
$81,583 $491
-
Tgal
TOTAL IMPLEMENTED $255,200 $165,031 $14,669
289,310
kWh
$158,948
-
MMBtu
$81,583 -
Yearly Savings* Imp'd Cost* Electricity Usage Savings Natural Gas Savings Administrative Changes Savings Water Consumption Savings
*Savings and costs are best estimates based on the center's site visit, associated engineering analysis, and typical capital and labor costs