Assessment Year | 1995 |
---|---|
Principal Product | Recreational Vehicles |
NAICS |
n/a
|
SIC | 3799: Transportation Equipment, Not Elsewhere Classified |
Sales Range | $50 M to 100M |
# of Employees | 450 |
Plant Area |
621,100
ft2
|
Annual Production | 50,000
pieces
|
Production Hrs. Annual | 6,000
hrs
|
Location (State) | Georgia |
Facility Energy Cost and Usage
Source | Yearly Cost | Usage | Unit Cost | |
---|---|---|---|---|
Electricity Usage | $1,222,210 | 23,038,687 |
kWh
|
$0.053 |
Natural Gas | $208,557 | 66,269 |
MMBtu
|
$3.15 |
TOTAL YEARLY COSTS | - | |||
RECOMMENDED SAVINGS* | $358,350 |
See individual recommendations below
*Non-energy impacts included in savings.
|
||
IMPLEMENTED SAVINGS* | $36,300 |
Recommendations
# | Description | Yearly Savings* | Imp'd Cost* | Status | Electricity Usage Savings | Natural Gas Savings | Solid Waste (non-haz) Savings |
---|---|---|---|---|---|---|---|
01 | 2.4133: Use most efficient type of electric motors | $10,700 | $85,490 |
$10,700
218,347
kWh
|
- | - | |
02 | 2.4111: Utilize energy-efficient belts and other improved mechanisms | $10,300 | $5,300 |
$10,300
213,951
kWh
|
- | - | |
03 | 2.4236: Eliminate leaks in inert gas and compressed air lines/ valves | $4,300 | $1,300 |
$4,300
90,270
kWh
|
- | - | |
04 | 2.7111: Reduce illumination to minimum necessary levels | $10,100 | $8,480 |
$10,100
212,485
kWh
|
- | - | |
05 | 2.1113: Reduce combustion air flow to optimum | $8,570 | $750 | - |
$8,570
-
MMBtu
|
- | |
06 | 2.4314: Use synthetic lubricant | $3,350 | - |
$3,350
55,686
kWh
|
- | - | |
07 | 2.7111: Reduce illumination to minimum necessary levels | $3,770 | $320 |
$3,770
63,013
kWh
|
- | - | |
08 | 2.7144: Install spectral reflectors / delamp | $8,960 | $31,380 |
$8,960
187,866
kWh
|
- | - | |
09 | 2.4224: Upgrade controls on compressors | $25,500 | $6,300 |
$25,500
533,411
kWh
|
- | - | |
10 | 3.2123: Convert to high volume low pressure (hvlp) paint guns | $272,800 | $20,800 | - | - |
$272,800
-
lb
|
|
TOTAL RECOMMENDED | $358,350 | $160,120 |
$76,980
1,575,029
kWh
|
$8,570
-
MMBtu
|
$272,800
-
lb
|
||
TOTAL IMPLEMENTED | $36,300 | $119,240 |
$27,730
559,496
kWh
|
$8,570
-
MMBtu
|
- | ||
Yearly Savings* | Imp'd Cost* | Electricity Usage Savings | Natural Gas Savings | Solid Waste (non-haz) Savings |
*Savings and costs are best estimates based on the center's site visit, associated engineering analysis, and typical capital and labor costs