Assessment Year | 1982 |
---|---|
Principal Product | TEXTILE FIBERS |
NAICS |
n/a
|
SIC | 2284: Thread Mills |
Sales Range | $1 M to 5M |
# of Employees | 70 |
Plant Area |
n/a
|
Annual Production | 24,501,613
pieces
|
Production Hrs. Annual | 4,590
hrs
|
Location (State) | Georgia |
Facility Energy Cost and Usage
Source | Yearly Cost | Usage | Unit Cost | |
---|---|---|---|---|
Electricity Usage | $190,273 | 3,731,829 |
kWh
|
$0.051 |
Natural Gas | $19,667 | 4,194 |
MMBtu
|
$4.69 |
Fuel Oil #2 | $4,673 | 727 |
MMBtu
|
$6.43 |
TOTAL YEARLY COSTS | - | |||
RECOMMENDED SAVINGS* | $9,950 |
See individual recommendations below
*Non-energy impacts included in savings.
|
||
IMPLEMENTED SAVINGS* | - |
Recommendations
# | Description | Yearly Savings* | Imp'd Cost* | Status | Electricity Usage Savings | Natural Gas Savings |
---|---|---|---|---|---|---|
01 | 2.4133: Use most efficient type of electric motors | $4,259 | $3,480 |
$4,259
83,529
kWh
|
- | |
02 | 2.4236: Eliminate leaks in inert gas and compressed air lines/ valves | $2,599 | $30 |
$2,599
50,996
kWh
|
- | |
03 | 2.2135: Repair and eliminate steam leaks | $960 | $60 | - |
$960
-
MMBtu
|
|
04 | 2.7142: Utilize higher efficiency lamps and/or ballasts | $674 | $330 |
$674
13,189
kWh
|
- | |
05 | 2.7142: Utilize higher efficiency lamps and/or ballasts | $403 | $154 |
$403
7,913
kWh
|
- | |
06 | 2.1233: Analyze flue gas for proper air/fuel ratio | $666 | $300 | - |
$666
-
MMBtu
|
|
07 | 2.2511: Insulate bare equipment | $389 | $244 | - |
$389
-
MMBtu
|
|
TOTAL RECOMMENDED | $9,950 | $4,598 |
$7,935
155,627
kWh
|
$2,015
-
MMBtu
|
||
TOTAL IMPLEMENTED | - | - | - | - | ||
Yearly Savings* | Imp'd Cost* | Electricity Usage Savings | Natural Gas Savings |
*Savings and costs are best estimates based on the center's site visit, associated engineering analysis, and typical capital and labor costs