ITAC Assessment: DL0120
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ITAC Assessment: DL0120
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Assessment Year 2014
Principal Product Mushrooms
NAICS 111411: Mushroom Production
SIC 0182: Food Crops Grown Under Cover
Sales Range $500
k
to 1
M
# of Employees 100
Plant Area 220,000
ft2
Annual Production 200,000,000
lb
Production Hrs. Annual 8,760
hrs
Location (State) Maryland

Facility Energy Cost and Usage

Source Yearly Cost Usage
Electricity Usage $785,939 8,664,000
kWh
Fuel Oil #2 $543,411 24,199
MMBtu
TOTAL YEARLY COSTS -
RECOMMENDED SAVINGS* $717,670 *Non-energy impacts included in savings.
IMPLEMENTED SAVINGS* $21,541

Recommendations

# Description Yearly Savings* Imp'd Cost* Status Electricity Usage Savings Fuel Oil #2 Savings
01 2.7135: Install occupancy sensors $62,900 $38,400 $62,900
691,100
kWh
-
02 2.7142: Utilize higher efficiency lamps and/or ballasts $16,777 $116,160 $16,777
184,365
kWh
-
03 2.7142: Utilize higher efficiency lamps and/or ballasts $1,734 $9,000 $1,734
19,053
kWh
-
04 2.2441: Preheat boiler makeup water with waste process heat $176,850 $624,000 $176,850
1,943,400
kWh
-
05 2.2437: Recover waste heat from equipment $338,000 $400,000 - $338,000
-
MMBtu
06 2.1123: Install automatic stack damper $22,042 $16,000 - $22,042
-
MMBtu
07 2.1221: Replace obsolete burners with more efficient ones $44,085 $50,000 - $44,085
-
MMBtu
08 2.2628: Utilize a less expensive cooling method $52,252 $500,000 $52,252
574,200
kWh
-
09 2.4236: Eliminate leaks in inert gas and compressed air lines/ valves $1,260 $300 $1,260
13,840
kWh
-
10 2.2113: Repair or replace steam traps $1,770 $350 - $1,770
-
MMBtu
TOTAL RECOMMENDED $717,670 $1,754,210 $311,773
3,425,958
kWh
$405,897
-
MMBtu
TOTAL IMPLEMENTED $21,541 $125,810 $19,771
217,258
kWh
$1,770
-
MMBtu
Yearly Savings* Imp'd Cost* Electricity Usage Savings Fuel Oil #2 Savings
*Savings and costs are best estimates based on the center's site visit, associated engineering analysis, and typical capital and labor costs