Assessment Year | 1987 |
---|---|
Principal Product | PRECAST CONCRETE |
NAICS |
n/a
|
SIC | 3272: Concrete Products, Except Block and Brick |
Sales Range | $10 M to 50M |
# of Employees | 250 |
Plant Area |
n/a
|
Annual Production | 8,078
thousand feet
|
Production Hrs. Annual | 6,240
hrs
|
Location (State) | Colorado |
Facility Energy Cost and Usage
Source | Yearly Cost | Usage | Unit Cost | |
---|---|---|---|---|
Electricity Usage | $128,712 | 1,417,937 |
kWh
|
$0.091 |
Natural Gas | $198,049 | 49,791 |
MMBtu
|
$3.98 |
TOTAL YEARLY COSTS | - | |||
RECOMMENDED SAVINGS* | $98,890 |
See individual recommendations below
*Non-energy impacts included in savings.
|
||
IMPLEMENTED SAVINGS* | $80,855 |
Recommendations
# | Description | Yearly Savings* | Imp'd Cost* | Status | Electricity Usage Savings | Natural Gas Savings |
---|---|---|---|---|---|---|
01 | 2.1233: Analyze flue gas for proper air/fuel ratio | $12,235 | $300 | - |
$12,235
-
MMBtu
|
|
02 | 2.2135: Repair and eliminate steam leaks | $8,294 | $3,331 | - |
$8,294
-
MMBtu
|
|
03 | 2.1222: Install turbulators | $5,059 | $1,700 | - |
$5,059
-
MMBtu
|
|
04 | 2.2136: Install / repair insulation on steam lines | $7,419 | $16,669 | - |
$7,419
-
MMBtu
|
|
05 | 2.2414: Use waste heat from hot flue gases to preheat | $10,077 | $16,800 | - |
$10,077
-
MMBtu
|
|
06 | 2.4236: Eliminate leaks in inert gas and compressed air lines/ valves | $7,421 | $400 |
$7,421
81,770
kWh
|
- | |
07 | 2.4312: Improve lubrication practices | $1,968 | - |
$1,968
21,688
kWh
|
- | |
08 | 2.2437: Recover waste heat from equipment | $784 | $200 | - |
$784
-
MMBtu
|
|
09 | 2.1311: Replace electrically-operated equipment with fossil fuel equipment | $24,041 | $70 |
$24,451
24,033
kWh
|
$(-410.0)
-
MMBtu
|
|
10 | 2.6242: Minimize operation of equipment maintained in standby condition | $18,372 | $500 | - |
$18,372
-
MMBtu
|
|
11 | 2.4133: Use most efficient type of electric motors | $372 | $869 |
$372
4,103
kWh
|
- | |
12 | 2.6218: Turn off equipment when not in use | $2,289 | $700 | - |
$2,289
-
MMBtu
|
|
13 | 2.7142: Utilize higher efficiency lamps and/or ballasts | $559 | $589 |
$559
6,155
kWh
|
- | |
TOTAL RECOMMENDED | $98,890 | $42,128 |
$34,771
137,749
kWh
|
$64,119
-
MMBtu
|
||
TOTAL IMPLEMENTED | $80,855 | $22,170 |
$31,872
105,803
kWh
|
$48,983
-
MMBtu
|
||
Yearly Savings* | Imp'd Cost* | Electricity Usage Savings | Natural Gas Savings |
*Savings and costs are best estimates based on the center's site visit, associated engineering analysis, and typical capital and labor costs