| Assessment Year | 1998 |
|---|---|
| Principal Product | Metal Shop |
| NAICS |
n/a
|
| SIC | 3599: Industrial and Commercial Machinery and Equipment, Not Elsewhere Classified |
| Sales Range | $10 M to 50M |
| # of Employees | 60 |
| Plant Area |
40,000
ft2
|
| Annual Production | 33
ton
|
| Production Hrs. Annual | 6,300
hrs
|
| Location (State) | Arizona |
Facility Energy Cost and Usage
| Source | Yearly Cost | Usage | Unit Cost | |
|---|---|---|---|---|
| Electricity Usage | $69,280 | 1,098,183 |
kWh
|
$0.063 |
| Electricity Demand | $8,750 | 3,176 |
kW-mo/yr
|
$2.76 |
| Electricity Fees | $4,215 | - |
|
- |
| TOTAL YEARLY COSTS | - | |||
| RECOMMENDED SAVINGS* | $163,002 |
See individual recommendations below
*Non-energy impacts included in savings.
|
||
| IMPLEMENTED SAVINGS* | - | |||
Recommendations
| # | Description | Yearly Savings* | Imp'd Cost* | Status | Electricity Usage Savings | Electricity Demand Savings | Solid Waste (non-haz) Savings | Personnel Changes Savings | Administrative Changes Savings | Primary Product Savings |
|---|---|---|---|---|---|---|---|---|---|---|
| 01 | 2.4231: Reduce the pressure of compressed air to the minimum required | $885 | $60 |
$814
14,947
kWh
|
$71
-
kW-mo/yr
|
- | - | - | - | |
| 02 | 2.7135: Install occupancy sensors | $385 | $675 |
$294
5,275
kWh
|
$91
-
kW-mo/yr
|
- | - | - | - | |
| 03 | 2.4146: Use adjustable frequency drive or multiple speed motors on existing system | $1,253 | $2,300 |
$1,253
22,860
kWh
|
- | - | - | - | - | |
| 04 | 2.7142: Utilize higher efficiency lamps and/or ballasts | $171 | $261 |
$152
2,931
kWh
|
$19
-
kW-mo/yr
|
- | - | - | - | |
| 05 | 2.7224: Reduce space conditioning during non-working hours | $505 | $675 |
$505
9,379
kWh
|
- | - | - | - | - | |
| 06 | 3.6192: Use a less expensive method of waste removal | $936 | $60 | - | - |
$936
-
lb
|
- | - | - | |
| 07 | 2.8114: Change rate schedules or other changes in utility service | $603 | $30 | - | - | - | - | $603 | - | |
| 08 | 4.111: Add equipment/ operators to reduce production bottleneck | $158,264 | $128,600 |
$(-9,281.0)
(-170,281)
kWh
|
$(-2,555.0)
-
kW-mo/yr
|
- | $(-157,500.0) | - | $327,600 | |
| TOTAL RECOMMENDED | $163,002 | $132,661 |
$(-6,263.0)
(-114,889)
kWh
|
$(-2,374.0)
-
kW-mo/yr
|
$936
-
lb
|
$(-157,500.0) | $603 | $327,600 | ||
| TOTAL IMPLEMENTED | - | - | - | - | - | - | - | - | ||
| Yearly Savings* | Imp'd Cost* | Electricity Usage Savings | Electricity Demand Savings | Solid Waste (non-haz) Savings | Personnel Changes Savings | Administrative Changes Savings | Primary Product Savings | |||
*Savings and costs are best estimates based on the center's site visit, associated engineering analysis, and typical capital and labor costs