Assessment Year | 1992 |
---|---|
Principal Product | PORTLAND CEMENT |
NAICS |
n/a
|
SIC | 3241: Cement, Hydraulic |
Sales Range | $10 M to 50M |
# of Employees | 130 |
Plant Area |
n/a
|
Annual Production | 700,000
ton
|
Production Hrs. Annual | 8,234
hrs
|
Location (State) | Arizona |
Facility Energy Cost and Usage
Source | Yearly Cost | Usage | Unit Cost | |
---|---|---|---|---|
Electricity Usage | $5,100,141 | 91,808,032 |
kWh
|
$0.056 |
Coal | $4,657,858 | 6,803,911 |
MMBtu
|
$0.68 |
TOTAL YEARLY COSTS | - | |||
RECOMMENDED SAVINGS* | $837,754 |
See individual recommendations below
*Non-energy impacts included in savings.
|
||
IMPLEMENTED SAVINGS* | $837,754 |
Recommendations
# | Description | Yearly Savings* | Imp'd Cost* | Status | Electricity Usage Savings | Natural Gas Savings | Administrative Changes Savings |
---|---|---|---|---|---|---|---|
01 | 2.4133: Use most efficient type of electric motors | $3,012 | $24,872 |
$3,012
54,220
kWh
|
- | - | |
02 | 2.4146: Use adjustable frequency drive or multiple speed motors on existing system | $345,320 | $530,000 |
$345,320
6,216,589
kWh
|
- | - | |
03 | 2.7142: Utilize higher efficiency lamps and/or ballasts | $2,583 | $8,109 |
$2,774
49,824
kWh
|
- | $(-191.0) | |
04 | 2.7142: Utilize higher efficiency lamps and/or ballasts | $1,446 | $3,248 |
$1,446
26,084
kWh
|
- | - | |
05 | 2.7142: Utilize higher efficiency lamps and/or ballasts | $4,462 | $7,288 |
$4,462
80,305
kWh
|
- | - | |
06 | 2.3412: Use waste heat to produce steam to drive a steam turbine-generator | $236,795 | $750,000 |
$324,395
5,839,977
kWh
|
- | $(-87,600.0) | |
07 | 2.8113: Purchase gas directly from a contract gas supplier | $107,027 | $6,700 | - |
$107,027
-
MMBtu
|
- | |
08 | 2.3415: Use a fossil fuel engine to cogenerate electricity or motive power; and utilize heat | $129,176 | $640,000 |
$364,057
6,547,186
kWh
|
$(-169,409.0)
-
MMBtu
|
$(-65,472.0) | |
09 | 2.4236: Eliminate leaks in inert gas and compressed air lines/ valves | $7,933 | $2,000 |
$7,933
142,732
kWh
|
- | - | |
TOTAL RECOMMENDED | $837,754 | $1,972,217 |
$1,053,399
18,956,917
kWh
|
$(-62,382.0)
-
MMBtu
|
$(-153,263.0) | ||
TOTAL IMPLEMENTED | $837,754 | $1,972,217 |
$1,053,399
18,956,917
kWh
|
$(-62,382.0)
-
MMBtu
|
$(-153,263.0) | ||
Yearly Savings* | Imp'd Cost* | Electricity Usage Savings | Natural Gas Savings | Administrative Changes Savings |
*Savings and costs are best estimates based on the center's site visit, associated engineering analysis, and typical capital and labor costs