| Assessment Year | 1995 |
|---|---|
| Principal Product | Vanadium Chemicals |
| NAICS |
n/a
|
| SIC | 2819: Industrial Inorganic Chemicals, Not Elsewhere Classified |
| Sales Range | $5 M to 10M |
| # of Employees | 66 |
| Plant Area |
250,000
ft2
|
| Annual Production | 3,000,000
lb
|
| Production Hrs. Annual | 6,048
hrs
|
| Location (State) | Arkansas |
Facility Energy Cost and Usage
| Source | Yearly Cost | Usage | Unit Cost | |
|---|---|---|---|---|
| Electricity Usage | $621,507 | 11,690,504 |
kWh
|
$0.053 |
| Natural Gas | $596,046 | 243,606 |
MMBtu
|
$2.45 |
| TOTAL YEARLY COSTS | - | |||
| RECOMMENDED SAVINGS* | $46,306 |
See individual recommendations below
*Non-energy impacts included in savings.
|
||
| IMPLEMENTED SAVINGS* | $46,306 | |||
Recommendations
| # | Description | Yearly Savings* | Imp'd Cost* | Status | Electricity Usage Savings | Natural Gas Savings |
|---|---|---|---|---|---|---|
| 01 | 2.1233: Analyze flue gas for proper air/fuel ratio | $13,281 | $1,000 | - |
$13,281
-
MMBtu
|
|
| 02 | 2.7111: Reduce illumination to minimum necessary levels | $2,889 | $400 |
$2,889
29,601
kWh
|
- | |
| 03 | 2.4133: Use most efficient type of electric motors | $5,741 | $9,240 |
$5,741
55,100
kWh
|
- | |
| 04 | 2.2135: Repair and eliminate steam leaks | $7,194 | $1,000 | - |
$7,194
-
MMBtu
|
|
| 05 | 2.4111: Utilize energy-efficient belts and other improved mechanisms | $5,687 | $885 |
$5,687
99,062
kWh
|
- | |
| 06 | 2.7142: Utilize higher efficiency lamps and/or ballasts | $11,514 | $1,109 |
$11,514
126,905
kWh
|
- | |
| TOTAL RECOMMENDED | $46,306 | $13,634 |
$25,831
310,668
kWh
|
$20,475
-
MMBtu
|
||
| TOTAL IMPLEMENTED | $46,306 | $13,634 |
$25,831
310,668
kWh
|
$20,475
-
MMBtu
|
||
| Yearly Savings* | Imp'd Cost* | Electricity Usage Savings | Natural Gas Savings | |||
*Savings and costs are best estimates based on the center's site visit, associated engineering analysis, and typical capital and labor costs