Assessment Year | 1994 |
---|---|
Principal Product | Inner Tubes & Bladders |
NAICS |
n/a
|
SIC | 3011: Tires and Inner Tubes |
Sales Range | $10 M to 50M |
# of Employees | 173 |
Plant Area |
200,000
ft2
|
Annual Production | 15,826,559
lb
|
Production Hrs. Annual | 6,257
hrs
|
Location (State) | Arkansas |
Facility Energy Cost and Usage
Source | Yearly Cost | Usage | Unit Cost | |
---|---|---|---|---|
Electricity Usage | $834,889 | 11,629,250 |
kWh
|
$0.072 |
Natural Gas | $264,498 | 88,496 |
MMBtu
|
$2.99 |
TOTAL YEARLY COSTS | - | |||
RECOMMENDED SAVINGS* | $90,894 |
See individual recommendations below
*Non-energy impacts included in savings.
|
||
IMPLEMENTED SAVINGS* | $38,947 |
Recommendations
# | Description | Yearly Savings* | Imp'd Cost* | Status | Electricity Usage Savings | Natural Gas Savings |
---|---|---|---|---|---|---|
01 | 2.4236: Eliminate leaks in inert gas and compressed air lines/ valves | $9,832 | $450 |
$9,832
136,870
kWh
|
- | |
02 | 2.7142: Utilize higher efficiency lamps and/or ballasts | $4,270 | $1,996 |
$4,270
59,496
kWh
|
- | |
03 | 2.2135: Repair and eliminate steam leaks | $8,858 | $2,200 | - |
$8,858
-
MMBtu
|
|
04 | 2.7111: Reduce illumination to minimum necessary levels | $15,987 | $1,177 |
$15,987
222,743
kWh
|
- | |
05 | 2.3131: Reschedule plant operations or reduce load to avoid peaks | $29,704 | - |
$29,704
-
kWh
|
- | |
06 | 2.7232: Replace existing hvac unit with high efficiency model | $22,243 | $47,000 |
$22,243
309,789
kWh
|
- | |
TOTAL RECOMMENDED | $90,894 | $52,823 |
$82,036
728,898
kWh
|
$8,858
-
MMBtu
|
||
TOTAL IMPLEMENTED | $38,947 | $5,823 |
$30,089
419,109
kWh
|
$8,858
-
MMBtu
|
||
Yearly Savings* | Imp'd Cost* | Electricity Usage Savings | Natural Gas Savings |
*Savings and costs are best estimates based on the center's site visit, associated engineering analysis, and typical capital and labor costs