| Assessment Year | 1993 |
|---|---|
| Principal Product | downhole drilling and fishing tools |
| NAICS |
n/a
|
| SIC | 3533: Oil and Gas Field Machinery and Equipment |
| Sales Range | $10 M to 50M |
| # of Employees | 157 |
| Plant Area |
30,000
ft2
|
| Annual Production | 600
pieces
|
| Production Hrs. Annual | 6,024
hrs
|
| Location (State) | Texas |
Facility Energy Cost and Usage
| Source | Yearly Cost | Usage | Unit Cost | |
|---|---|---|---|---|
| Electricity Usage | $160,895 | 1,842,614 |
kWh
|
$0.087 |
| Natural Gas | $33,390 | 6,029 |
MMBtu
|
$5.54 |
| TOTAL YEARLY COSTS | - | |||
| RECOMMENDED SAVINGS* | $15,390 |
See individual recommendations below
*Non-energy impacts included in savings.
|
||
| IMPLEMENTED SAVINGS* | $8,930 | |||
Recommendations
| # | Description | Yearly Savings* | Imp'd Cost* | Status | Electricity Usage Savings | Natural Gas Savings |
|---|---|---|---|---|---|---|
| 01 | 2.7124: Make a practice of turning off lights when not needed | $6,460 | - |
$6,460
77,374
kWh
|
- | |
| 02 | 2.4226: Use / purchase optimum sized compressor | $3,950 | - |
$3,950
36,635
kWh
|
- | |
| 03 | 2.7235: Install fossil fuel make-up air unit | $890 | $460 | - |
$890
-
MMBtu
|
|
| 04 | 2.4236: Eliminate leaks in inert gas and compressed air lines/ valves | $2,720 | $420 |
$2,720
53,341
kWh
|
- | |
| 05 | 2.7142: Utilize higher efficiency lamps and/or ballasts | $1,370 | - |
$1,370
21,395
kWh
|
- | |
| TOTAL RECOMMENDED | $15,390 | $880 |
$14,500
188,745
kWh
|
$890
-
MMBtu
|
||
| TOTAL IMPLEMENTED | $8,930 | $880 |
$8,040
111,371
kWh
|
$890
-
MMBtu
|
||
*Savings and costs are best estimates based on the center's site visit, associated engineering analysis, and typical capital and labor costs