Assessment Year | 1992 |
---|---|
Principal Product | MILK |
NAICS |
n/a
|
SIC | 2026: Fluid Milk |
Sales Range | $10 M to 50M |
# of Employees | 260 |
Plant Area |
n/a
|
Annual Production | 3,744
Tgal
|
Production Hrs. Annual | 4,472
hrs
|
Location (State) | Texas |
Facility Energy Cost and Usage
Source | Yearly Cost | Usage | Unit Cost | |
---|---|---|---|---|
Electricity Usage | $183,457 | 3,338,804 |
kWh
|
$0.055 |
Natural Gas | $67,686 | 15,746 |
MMBtu
|
$4.30 |
TOTAL YEARLY COSTS | - | |||
RECOMMENDED SAVINGS* | $42,935 |
See individual recommendations below
*Non-energy impacts included in savings.
|
||
IMPLEMENTED SAVINGS* | - |
Recommendations
# | Description | Yearly Savings* | Imp'd Cost* | Status | Electricity Usage Savings | Natural Gas Savings |
---|---|---|---|---|---|---|
01 | 2.3512: De-energize excess transformer capacity | $23,665 | $13,890 | - |
$23,665
-
MMBtu
|
|
02 | 2.1212: Operate boilers on high fire setting | $6,790 | $6,500 | - |
$6,790
-
MMBtu
|
|
03 | 2.7142: Utilize higher efficiency lamps and/or ballasts | $5,300 | $5,610 |
$5,300
72,685
kWh
|
- | |
04 | 2.3131: Reschedule plant operations or reduce load to avoid peaks | $3,770 | $400 |
$3,770
-
kWh
|
- | |
05 | 2.6212: Turn off equipment during breaks, reduce operating time | $2,400 | - |
$2,400
55,686
kWh
|
- | |
06 | 2.4239: Eliminate or reduce compressed air usage | $1,010 | $1,080 |
$1,010
23,447
kWh
|
- | |
TOTAL RECOMMENDED | $42,935 | $27,480 |
$12,480
151,818
kWh
|
$30,455
-
MMBtu
|
||
TOTAL IMPLEMENTED | - | - | - | - | ||
Yearly Savings* | Imp'd Cost* | Electricity Usage Savings | Natural Gas Savings |
*Savings and costs are best estimates based on the center's site visit, associated engineering analysis, and typical capital and labor costs