| Assessment Year | 1992 |
|---|---|
| Principal Product | MILK |
| NAICS |
n/a
|
| SIC | 2026: Fluid Milk |
| Sales Range | $10 M to 50M |
| # of Employees | 260 |
| Plant Area |
n/a
|
| Annual Production | 3,744
Tgal
|
| Production Hrs. Annual | 4,472
hrs
|
| Location (State) | Texas |
Facility Energy Cost and Usage
| Source | Yearly Cost | Usage | Unit Cost | |
|---|---|---|---|---|
| Electricity Usage | $183,457 | 3,338,804 |
kWh
|
$0.055 |
| Natural Gas | $67,686 | 15,746 |
MMBtu
|
$4.30 |
| TOTAL YEARLY COSTS | - | |||
| RECOMMENDED SAVINGS* | $42,935 |
See individual recommendations below
*Non-energy impacts included in savings.
|
||
| IMPLEMENTED SAVINGS* | - | |||
Recommendations
| # | Description | Yearly Savings* | Imp'd Cost* | Status | Electricity Usage Savings | Natural Gas Savings |
|---|---|---|---|---|---|---|
| 01 | 2.3512: De-energize excess transformer capacity | $23,665 | $13,890 | - |
$23,665
-
MMBtu
|
|
| 02 | 2.1212: Operate boilers on high fire setting | $6,790 | $6,500 | - |
$6,790
-
MMBtu
|
|
| 03 | 2.7142: Utilize higher efficiency lamps and/or ballasts | $5,300 | $5,610 |
$5,300
72,685
kWh
|
- | |
| 04 | 2.3131: Reschedule plant operations or reduce load to avoid peaks | $3,770 | $400 |
$3,770
-
kWh
|
- | |
| 05 | 2.6212: Turn off equipment during breaks, reduce operating time | $2,400 | - |
$2,400
55,686
kWh
|
- | |
| 06 | 2.4239: Eliminate or reduce compressed air usage | $1,010 | $1,080 |
$1,010
23,447
kWh
|
- | |
| TOTAL RECOMMENDED | $42,935 | $27,480 |
$12,480
151,818
kWh
|
$30,455
-
MMBtu
|
||
| TOTAL IMPLEMENTED | - | - | - | - | ||
| Yearly Savings* | Imp'd Cost* | Electricity Usage Savings | Natural Gas Savings | |||
*Savings and costs are best estimates based on the center's site visit, associated engineering analysis, and typical capital and labor costs