ITAC Assessment: UF0086
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ITAC Assessment: UF0086
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Assessment Year 1994
Principal Product Corrugated boxes and sheets
NAICS
n/a
SIC 2653: Corrugated and Solid Fiber Boxes
Sales Range $10
M
to 50
M
# of Employees 125
Plant Area 194,000
ft2
Annual Production 504,000,000
pieces
Production Hrs. Annual 4,992
hrs
Location (State) Florida

Facility Energy Cost and Usage

Source Yearly Cost Usage
Electricity Usage $240,181 3,356,389
kWh
Natural Gas $137,064 32,412
MMBtu
TOTAL YEARLY COSTS -
RECOMMENDED SAVINGS* $32,444 *Non-energy impacts included in savings.
IMPLEMENTED SAVINGS* $13,647

Recommendations

# Description Yearly Savings* Imp'd Cost* Status Electricity Usage Savings Natural Gas Savings
01 2.7142: Utilize higher efficiency lamps and/or ballasts $3,091 $3,937 $3,091
42,790
kWh
-
02 2.7144: Install spectral reflectors / delamp $2,567 $3,210 $2,567
33,705
kWh
-
03 2.4133: Use most efficient type of electric motors $4,105 $4,519 $4,105
57,151
kWh
-
04 2.4111: Utilize energy-efficient belts and other improved mechanisms $1,382 $1,000 $1,382
19,050
kWh
-
05 2.1233: Analyze flue gas for proper air/fuel ratio $4,781 $1,000 - $4,781
-
MMBtu
06 2.2414: Use waste heat from hot flue gases to preheat $3,774 $2,600 - $3,774
-
MMBtu
07 2.2136: Install / repair insulation on steam lines $851 $610 - $851
-
MMBtu
08 2.4146: Use adjustable frequency drive or multiple speed motors on existing system $10,223 $23,300 $10,223
173,212
kWh
-
09 2.2135: Repair and eliminate steam leaks $1,670 $220 - $1,670
-
MMBtu
TOTAL RECOMMENDED $32,444 $40,396 $21,368
325,908
kWh
$11,076
-
MMBtu
TOTAL IMPLEMENTED $13,647 $9,676 $7,196
99,941
kWh
$6,451
-
MMBtu
Yearly Savings* Imp'd Cost* Electricity Usage Savings Natural Gas Savings
*Savings and costs are best estimates based on the center's site visit, associated engineering analysis, and typical capital and labor costs