Assessment Year | 1991 |
---|---|
Principal Product | POWER CABLE |
NAICS |
n/a
|
SIC | 3357: Drawing and Insulating of Nonferrous Wire |
Sales Range | $10 M to 50M |
# of Employees | 60 |
Plant Area |
n/a
|
Annual Production | 16
thousand feet
|
Production Hrs. Annual | 5,000
hrs
|
Location (State) | Oklahoma |
Facility Energy Cost and Usage
Source | Yearly Cost | Usage | Unit Cost | |
---|---|---|---|---|
Electricity Usage | $256,169 | 4,745,897 |
kWh
|
$0.054 |
Natural Gas | $26,610 | 9,242 |
MMBtu
|
$2.88 |
TOTAL YEARLY COSTS | - | |||
RECOMMENDED SAVINGS* | $75,169 |
See individual recommendations below
*Non-energy impacts included in savings.
|
||
IMPLEMENTED SAVINGS* | $75,169 |
Recommendations
# | Description | Yearly Savings* | Imp'd Cost* | Status | Electricity Usage Savings | Natural Gas Savings | Administrative Changes Savings |
---|---|---|---|---|---|---|---|
01 | 2.4239: Eliminate or reduce compressed air usage | $12,997 | $600 |
$12,997
225,967
kWh
|
- | - | |
02 | 2.3131: Reschedule plant operations or reduce load to avoid peaks | $56,160 | - |
$56,160
-
kWh
|
- | - | |
03 | 2.2135: Repair and eliminate steam leaks | $3,777 | - | - |
$3,827
-
MMBtu
|
$(-50.0) | |
04 | 2.1311: Replace electrically-operated equipment with fossil fuel equipment | $1,871 | - |
$2,008
10,551
kWh
|
$(-137.0)
-
MMBtu
|
- | |
05 | 2.2123: Insulate feedwater tank | $364 | $487 | - |
$364
-
MMBtu
|
- | |
TOTAL RECOMMENDED | $75,169 | $1,087 |
$71,165
236,518
kWh
|
$4,054
-
MMBtu
|
$(-50.0) | ||
TOTAL IMPLEMENTED | $75,169 | $1,087 |
$71,165
236,518
kWh
|
$4,054
-
MMBtu
|
$(-50.0) |
*Savings and costs are best estimates based on the center's site visit, associated engineering analysis, and typical capital and labor costs